Accident Beechcraft A36 N769LW,
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ASN Wikibase Occurrence # 202172
 
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Date:Wednesday 21 April 1999
Time:16:43 LT
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36
Owner/operator:Joseph W. Camp
Registration: N769LW
MSN: E1028
Engine model:Continental IO-520-BA
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Courtland, AL -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Houston, MS (M44)
Destination airport:Huntsville, AL (KHSV)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During cruise flight, throttle response was not possible and the engine rpm decreased to near idle. While descending for a forced landing with the landing gear extended, the pilot later stated that he could not recall the last several thousand feet of the descent. The airplane collided with trees then the ground. Postaccident examination of the airplane revealed a castellated nut which secures a lever onto the throttle plate shaft was loose by 10.5 turns of the 6 sided nut; no cotter pin was found. This condition would not allow movement of the throttle plate shaft with movement of the throttle control. Postaccident, the engine was removed from the airplane, placed in a test cell, and found to operate normally. Following collapse of the nose landing gear August 1998, the engine and fuel control valve were overhauled. Following the engine overhaul, the engine was test run. The air throttle assembly was then removed for shipping, the lever was loosened, and the engine and boxed air throttle assembly were shipped to where the airplane was being repaired. The air throttle assembly was installed on the engine which was installed into the airplane. The engine was then run and no engine related discrepancies were noted.

Probable Cause: The failure of maintenance personnel from Signature Flight Support to assure that a cotter pin was installed at the air throttle assembly lever following installation of the overhauled fuel control valve onto the overhauled engine. This resulted in the partial loss of engine power due to the failure of the pilot to adjust the throttle control. A factor in the accident was the premature extension by the pilot of the landing gear which reduced the glide distance.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA99LA137
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB MIA99LA137

Location

Revision history:

Date/timeContributorUpdates
26-Nov-2017 12:42 ASN Update Bot Added
08-Apr-2024 06:51 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Destination airport, Source, Narrative, Category, Accident report]

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