ASN Wikibase Occurrence # 202186
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Date: | Wednesday 7 April 1999 |
Time: | 10:45 LT |
Type: | Cessna 172N |
Owner/operator: | Curtis E. Brewer |
Registration: | N5171K |
MSN: | 73998 |
Total airframe hrs: | 8019 hours |
Engine model: | Lycoming O-320-H2AD |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Turrell, AR -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Training |
Departure airport: | Memphis, TN (MO1) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While maneuvering at a low altitude, there was a loss of engine power. During the forced landing to a rough/uneven road, the airplane's right main tire exited the road into a muddy ditch. The airplane nosed down in the adjacent soft field. Postaccident investigation revealed that the #1 cylinder intake valve rocker assembly stud bolt was backed out of the hole four turns, allowing the valve to become inoperative. Lycoming service bulletin 412B issued in March 1978, for replacing all rocker arm retaining studs with oversized studs was complied with at the factory before engine S/N L-7296-76 was shipped to Cessna in 1979. The original logbooks were reported lost; therefore, the complete history of the engine could not be verified. A review of reconstructed logbooks revealed that on February 12, 1998, the engine had accumulated '200 to 300 hours' since major overhaul. A 100-hour inspection maintenance entry for September 24, 1998, stated in part: 'Removed #1 cylinder, honed and installed new rings. #1 compression checked 68/80 at ground run. This engine determined to be in an airworthy condition.'
Probable Cause: The total loss of engine power as the result of improper maintenance which led to the number one cylinder intake valve rocker assembly stud bolt backing out rendering the valve inoperative. A factor was the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW99LA110 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB FTW99LA110
Location
Revision history:
Date/time | Contributor | Updates |
26-Nov-2017 12:42 |
ASN Update Bot |
Added |
08-Apr-2024 07:35 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report] |
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