ASN Wikibase Occurrence # 207118
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Date: | Monday 5 March 2018 |
Time: | 14:30 LT |
Type: | Mac Cub |
Owner/operator: | Private |
Registration: | N669WH |
MSN: | 001 |
Year of manufacture: | 2005 |
Total airframe hrs: | 290 hours |
Engine model: | Lycoming O-360-A4G |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Davis County, West Point, UT -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Ogden, UT |
Destination airport: | Ogden, UT |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and pilot rated passenger were conducting a local flight when the engine began to run roughly, and partial loss of engine power followed. The airplane was unable to maintain altitude, and the pilot made a forced landing onto a muddy road. During the landing roll, the airplane sunk in the mud, nosed over, and came to rest inverted, causing substantial damage to the left wing and vertical stabilizer. An engine examination and test run were performed, which revealed no preaccident mechanical failures or malfunctions that would have precluded normal operation.
The nearest weather reporting facility, located about 6 nautical miles from the accident site, reported a temperature of 35.6oF and a dew point of 19.4oF, which was in the range of atmosphere conditions that are conducive to carburetor icing at glide and cruise power settings. The pilot reported that the carburetor heat was not activated at the time of the partial loss of engine power.
The pilot also reported that he was in the rear airplane seat. Although the pilot had access to both sets of flight controls, the rear seat compartment was not equipped with a carburetor heat control handle. Engine power would likely have been restored if the carburetor heat had been engaged.
Probable Cause: The pilot's failure to use carburetor heat during the flight, which resulted in a partial loss of engine power due to carburetor icing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR18LA102 |
Status: | Investigation completed |
Duration: | 4 years |
Download report: | Final report |
|
Sources:
NTSB WPR18LA102
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=669WH Location
Revision history:
Date/time | Contributor | Updates |
06-Mar-2018 17:00 |
Geno |
Added |
02-Jul-2022 17:49 |
ASN Update Bot |
Updated [Time, Total occupants, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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