Runway excursion Accident Cessna 150E N6250T,
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ASN Wikibase Occurrence # 210303
 
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Date:Wednesday 20 September 2017
Time:15:30
Type:Silhouette image of generic C150 model; specific model in this crash may look slightly different    
Cessna 150E
Owner/operator:Private
Registration: N6250T
MSN: 15060950
Year of manufacture:1964
Total airframe hrs:6162 hours
Engine model:Continental O-200 SERIES
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Siler City, NC -   United States of America
Phase: En route
Nature:Private
Departure airport:Lexington, NC (EXX)
Destination airport:Lexington, NC (EXX)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, during a time-building, cross-country flight, the airplane had multiple mechanical malfunctions. On the fourth leg of the flight, he departed the airport and noticed that the airplane was low on fuel. He flew to a nearby airport, landed, and added 10 gallons of fuel.
After fueling, the airplane would not start, and the pilot asked maintenance personnel to jump the airplane’s battery. Then, during taxi to the runway, he noticed that the “radios and other electronics” were inoperative, but he continued to the runway. During the takeoff roll, he was startled by a loud noise in his headset, which he believed came from the airplane’s communication radio. He attempted to assess the problem during the takeoff roll, and the airplane veered off the right side of the runway into the safety area.
After regaining control, he taxied back to the approach end of the runway. He performed a flight control check and an engine power check and departed the airport.
The pilot reported that he then landed at a nontowered airport “to check out the aircraft.” He performed another flight control check and an engine run-up but did not exit the airplane “because of the starting issue.” The pilot then departed for the destination airport. He reported that he landed the airplane and taxied to parking. He recalled that he performed a postflight check of the airplane, but “other than grass and grass stains [he] did not see any damage.”
Later that evening, the airplane’s owner informed the pilot that the left wing was damaged.
The airplane sustained substantial damage to the left-wing spar and aileron. 



Probable Cause: The pilot’s improper decision to take off with known electrical issues, which distracted him and led to a loss of directional control during the takeoff roll.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: GAA17CA546
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
01-May-2018 13:45 ASN Update Bot Added

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