ASN Wikibase Occurrence # 212782
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Date: | Saturday 30 June 2018 |
Time: | 11:55 |
Type: | Cessna 337F Super Skymaster |
Owner/operator: | Private |
Registration: | N107BL |
MSN: | 33701330 |
Year of manufacture: | 1970 |
Total airframe hrs: | 2918 hours |
Engine model: | Continental IO-360-C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Vinland Valley Aerodrome (K64), Baldwin City, KS -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Baldwin City, KS (K64) |
Destination airport: | Baldwin City, KS (K64) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was conducting a local flight to practice single-engine maneuvers. After taking off and climbing the airplane to 3,500 ft, he shut down the rear engine and feathered the propeller. After performing some turns and climbs, the pilot attempted to unfeather the propeller and restart the engine but was unsuccessful. He returned to the airport to set up for a single-engine approach. During the approach, the pilot realized that the flaps were no longer in the full-flap setting and that a landing on the grass runway was going to be close, so he chose to perform a go-around. However, as the pilot began to go around, he realized that the airplane could not maintain altitude. He maneuvered the airplane for an off-airport landing to a nearby field, during which the airplane struck small trees and a fence and sustained substantial damage to the left wing and fuselage.
The rear engine propeller had a remote hydraulic accumulator that assisted in unfeathering the propeller and was normally serviced to 120 pounds per square inch (psi). During an annual inspection that took place 4 flight hours before the accident flight, it was noted that the pressure was slightly low. During postaccident examination, the accumulator pressure was 85 psi. It is likely that a nitrogen leak occurred between the time the accumulator was last serviced and the time of the accident; however, the reason for the nitrogen leak could not be determined. Further, the flap switch was not holding position due to a loss of tension at the flap switch pivot, which is likely why the flaps were not in the full-flap setting as reported by the pilot.
Probable Cause: The loss of hydraulic accumulator pressure for reasons that could not be determined, which prevented the propeller from unfeathering, and the pilot's improper decision to attempt a go-around, which resulted in an off-airport landing and the airplane impacting trees and a fence. Contributing to the accident was the loss of tension at the flap switch pivot, which prevented it from holding position.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN18LA246 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=107BL Location
Revision history:
Date/time | Contributor | Updates |
01-Jul-2018 18:40 |
Captain Adam |
Added |
01-Jul-2018 21:09 |
Geno |
Updated [Time, Location, Phase, Nature, Departure airport, Destination airport, Source] |
04-Jul-2018 01:11 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Location, Phase, Source, Narrative] |
22-Apr-2020 17:02 |
ASN Update Bot |
Updated [Time, Operator, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Accident report, ] |
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