ASN Wikibase Occurrence # 213087
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Date: | Sunday 8 July 2018 |
Time: | 06:43 LT |
Type: | Best Off Skyranger |
Owner/operator: | Private |
Registration: | N4329R |
MSN: | 481 |
Year of manufacture: | 2002 |
Total airframe hrs: | 292 hours |
Engine model: | Rotax 582 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Houghton Lake State Airport (5Y2), Houghton Lake Heights, MI -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Houghton Lake, MI |
Destination airport: | Houghton Lake, MI |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting a local private flight when the airplane had a sudden loss of engine power shortly after takeoff. The pilot reported that after an uneventful takeoff, as the airplane climbed through 150 ft above ground level, the engine speed rapidly decreased from 6,200 rpm to 4,700 rpm. Despite the pilot's corrective actions, the engine continued to operate at a decreased power setting and the airplane was unable to maintain altitude. The pilot reported that there were trees ahead of the airplane's flight path, so he turned into the wind and maneuvered to land on a nearby golf course fairway. The pilot stated that the airplane had insufficient altitude and airspeed to flare normally, which resulted in a hard landing and substantial damage to both wings and the empennage.
The pilot reported that he did not observe any anomalies during his preflight inspection or his before-takeoff engine runup, and that the fuel tank contained about 12 gallons of automotive fuel. A postaccident engine examination did not reveal any evidence of mechanical malfunctions or failures that would have precluded normal operation during the flight. Although the atmospheric conditions were conducive for the formation of carburetor icing, the airplane's engine was equipped with carburetors with a variable-venturi design that are generally not prone to carburetor icing. Therefore, the reason for the partial loss of engine power could not be determined with the available evidence.
Probable Cause: A partial loss of engine power during takeoff for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN18LA280 |
Status: | Investigation completed |
Duration: | 2 years and 10 months |
Download report: | Final report |
|
Sources:
NTSB CEN18LA280
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=4329R Location
Revision history:
Date/time | Contributor | Updates |
09-Jul-2018 03:23 |
Geno |
Added |
09-Jul-2018 03:24 |
Geno |
Updated [Source] |
10-Jul-2018 00:11 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source, Narrative] |
09-Jul-2022 05:42 |
ASN Update Bot |
Updated [Time, Cn, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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