ASN Wikibase Occurrence # 213480
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Date: | Thursday 19 July 2018 |
Time: | 08:02 |
Type: | Piper PA-28-140 Cherokee |
Owner/operator: | Private |
Registration: | N7080F |
MSN: | 28-7725-085 |
Year of manufacture: | 1976 |
Total airframe hrs: | 3301 hours |
Engine model: | Lycoming O-320-E3D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | N of Shreveport Downtown Airport (KDTN),, LA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Shreveport Downtown Airport, LA (DTN/KDTN) |
Destination airport: | Shreveport Downtown Airport, LA (DTN/KDTN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed on a postmaintenance check flight after an annual inspection on the previous day. According to the pilot, the airplane was flown in the local traffic pattern before departing the area. As the airplane climbed through 2,500 ft, it was not climbing more than 300 ft per minute without losing airspeed, and the pilot noticed a decrease in engine rpm. The pilot indicated that the oil pressure and oil temperature were normal, the vacuum gauge indicated "zero," and gyroscopic instruments began to drift and tumble. The pilot proceeded directly for the nearest airport, and when on final approach for the runway, the engine rpm and airspeed decreased. The engine did not respond to throttle inputs, and the pilot landed the airplane on a river levy. The airplane bounced, contacted a road, and came to rest against the airport perimeter fence, which resulted in substantial damage to both wings. Examination of the engine revealed that the output shaft of the vacuum pump was sheared. It could not be determined if the vacuum pump output shaft failed before or during the accident sequence. Additional engine information was not available. The reason for the partial loss of engine power could not be determined.
Probable Cause: The partial loss of engine power for reasons that could not be determined based on the available evidence.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN18LA281 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N7080F Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
19-Jul-2018 16:22 |
Geno |
Added |
19-Jul-2018 19:24 |
Aerossurance |
Updated [Location, Narrative] |
19-Jul-2018 19:56 |
Iceman 29 |
Updated [Source, Embed code] |
20-Jul-2018 07:27 |
Aerossurance |
Updated [Location, Embed code, Narrative] |
20-Jul-2018 10:16 |
RobertMB |
Updated [Aircraft type] |
22-Jul-2018 16:29 |
Anon. |
Updated [Embed code] |
23-Jul-2018 18:19 |
Anon. |
Updated [Total occupants, Narrative] |
08-Jun-2020 08:40 |
ASN Update Bot |
Updated [Time, Cn, Operator, Nature, Departure airport, Destination airport, Source, Embed code, Narrative, Accident report, ] |
08-Jun-2020 17:26 |
harro |
Updated [Departure airport, Destination airport, Source, Embed code, Narrative, Photo, Accident report, ] |
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