ASN Wikibase Occurrence # 213514
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 2 October 1970 |
Time: | 14:05 |
Type: | de Havilland Canada DHC-1 T Mk 10 Chipmunk |
Owner/operator: | Private |
Registration: | VH-AKB |
MSN: | |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Location: | Everglades Golf Course, Woy Woy, NSW -
Australia
|
Phase: | Landing |
Nature: | Private |
Departure airport: | YSBK |
Destination airport: | |
Investigating agency: | BASI |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While the aircraft was in flight at some 3000 feet above the Hawkesbury River, the VHF communications radio failed. After a few moments the pilot was aware of a smell of burning and he switched off the radio. Shortly after the radio was switched off, pungent smoke originating from the area of the radio installation under the instrument panel began to enter the cockpit and the pilot was compelled to open the canopy. He decided to land immediately and commenced an approach to a fairway on the nearby golf course. The approach was high and fast and the aircraft overshot the fairway. The pilot lowered full flap at approximately 90 knots and after crossing a line of trees proceeded to land on another fairway. Prior to touchdown he turned off the ignition, fuel and master switch and warned his passenger to leave the aircraft as soon as it stopped. When on short final the pilot noticed some golfers near the far end of the fairway and he applied full brake and full right rudder before touching down. The aircraft made contact with the ground initially on the right wing tip, bouncing on to the main wheels and nose before falling back on to the main undercarriage and tail wheel. The total ground run was 180 feet. Subsequent bench testing of VHF radio equipment revealed that in the circumstances of the filter capacitor breaking down, the overheating of the filter inductor produced smoke from the insulating substance.
Accident investigation:
|
| |
Investigating agency: | BASI |
Report number: | |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
https://www.atsb.gov.au/publications/investigation_reports/1970/aair/aair197001298/ https://www.atsb.gov.au/media/24578/197001298.pdf Revision history:
Date/time | Contributor | Updates |
20-Jul-2018 02:54 |
Pineapple |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation