ASN Wikibase Occurrence # 21511
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Date: | Thursday 26 June 2008 |
Time: | 17:56 |
Type: | Cessna 310R |
Owner/operator: | Marco Aviation, Inc |
Registration: | N4912A |
MSN: | 310R1399 |
Year of manufacture: | 1978 |
Total airframe hrs: | 8914 hours |
Engine model: | Continental IO-520-M1 |
Fatalities: | Fatalities: 0 / Occupants: 6 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gulf of Mexico, about six miles south of Goodland, FL -
United States of America
|
Phase: | En route |
Nature: | Passenger |
Departure airport: | Key West, FL (EYW) |
Destination airport: | Marco Island, FL (MKY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane experienced a total loss of engine power from both engines and was ditched in the Gulf of Mexico. According to pilot, after takeoff, the flight climbed briefly to 3,000 feet mean sea level (msl), descended to and remained at 2,500 feet msl, and then proceeded to the destination airport. When the flight was near the destination airport, the pilot reduced both throttles to 21 inches manifold pressure, and began descending at less than 500 feet-per-minute. Approximately 15 miles from the destination, while flying at 1,500 feet msl, the right engine "coughed a couple times" with corresponding right yaw. The pilot noted the right fuel flow was "down" and described a split between the left and right fuel flow readings. He reported that the left and right fuel quantity gauges indicated 70 and 100 pounds respectively, at a point just before the ditching. He turned the right auxiliary fuel pump to the low position, and moved the right fuel selector to the "left main" position in an effort to restore engine power; however, the right engine lost engine power, followed by the left engine. Following recovery of the airplane, a total of 14 ounces of fuel were drained from the left main fuel tank and no fuel was recovered from the right main fuel tank. Historical fuel records associated with the accident airplane revealed the average fuel burn was approximately 35.09 gallons-per-hour, the actual fuel load for the accident flight being only 119 pounds, instead of the pilot reported 280 pounds. The pilot did not visually inspect the fuel tanks. Rather, he relied on gauge readings and his fuel calculations, that amount only allowed approximately 34 minutes of flight at the typical power settings. Testing of components of the fuel quantity indicating system revealed no evidence of preimpact failure or malfunction. Both engines were operated postaccident with no preimpact failure or mechanical malfunction noted.
Probable Cause: The pilot’s inaccurate fuel consumption calculations, which resulted in a total loss of engine power to both engines due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA08LA128 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
29-Jun-2008 10:38 |
Fusko |
Added |
16-Jul-2008 01:26 |
Fusko |
Updated |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 11:19 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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