Incident Cessna 180G VH-DFO,
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ASN Wikibase Occurrence # 217905
 
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Date:Saturday 3 October 1987
Time:17:15
Type:Silhouette image of generic C180 model; specific model in this crash may look slightly different    
Cessna 180G
Owner/operator:
Registration: VH-DFO
MSN: 18051427
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: Substantial
Location:Berrigan, NSW -   Australia
Phase: Landing
Nature:Parachuting
Departure airport:Berrigan, NSW
Destination airport:Berrigan, NSW
Investigating agency: BASI
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While conducting parachute dropping runs from 5000 feet the pilot heard a loud bang from the engine and saw an object ejected through the top engine cowling. The windscreen was immediately covered with engine oil and the engine lost power. The parachutists abandoned the aircraft, and the pilot made a forced landing in a field of young wheat. The field sloped downwards in the direction of the landing roll, and the aircraft nosed-over when the main wheels intersected a shallow ditch while wheel brakes were being applied. Investigation revealed that the number 4 connecting rod had failed in fatigue across a big end arm. The fatigue had multiple origins on both the outside and inside of the arm, and propagated through approximately 95% of the cross-sectional area. The fatigue initiated from the inside of the big end bore revealed characteristics indicative of high cycle low stress fatigue, while the fatigue commencing from the outside of the arm propagated through high stress low cycle fatigue. The join between the two lines of propagation ran parallel with the bore. The other big end arm had 4 distinct fatigue initiations, one con-rod bolt had failed in overload with distinct signs of necking, while the other bolt remained attached to the cap and remaining part of the big end arm. The No.4 slipper bearing was reduced to a large quantity of severely deformed cold-worked fragments. Detailed metallurgical examination of the failed bearing did not disclose the cause of the failure. The oil filter was clogged with deposits and oil sludge. The bypass and pressure relief valve cavities contained similar deposits. The engine oil had the appearance of dirty used oil. However, laboratory analysis suggested that the oil had changed very little when compared with unused oil. The spark plugs were found to be oily, fouled and heavily deposited by carbon and lead. The aircraft had only flown 6 hours since the previous 100 hour inspection. This inspection should include the inspection of the oil filter, changing of the engine oil and servicing of spark plugs. The condition of the spark plugs was inconsistent with 6 hours of flight time. Approximations of the length of time for which the oil and plugs had been in use was not determined. Examination of the stripped engine disclosed that the oil passages were free, and no components showed signs of oil starvation. The cause of the bearing failure was not established.

Accident investigation:
cover
  
Investigating agency: BASI
Report number: 
Status: Investigation completed
Duration:
Download report: Final report

Sources:

https://www.atsb.gov.au/publications/investigation_reports/1987/aair/aair198702428/
https://www.atsb.gov.au/media/30237/aair198702428.pdf

Revision history:

Date/timeContributorUpdates
16-Nov-2018 09:37 Pineapple Added

Corrections or additions? ... Edit this accident description

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