ASN Wikibase Occurrence # 218679
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Date: | Thursday 27 August 2015 |
Time: | 12:00 |
Type: | Air Tractor AT-502B |
Owner/operator: | Red Willow Aviation Spraying Inc |
Registration: | N61267 |
MSN: | 502B-0303 |
Year of manufacture: | 1995 |
Engine model: | Walter M601E11 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Monroe, NE -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | Genoa, NE (97Y) |
Destination airport: | Genoa, NE (97Y) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was performing an aerial application flight when the airplane experienced a partial loss of engine power. The engine instruments showed that the engine was operating, but was producing less than idle power. The pilot applied full throttle with no effect. He subsequently turned the airplane into the wind, lowered the flaps, and when he heard corn hitting the bottom of the airplane, pulled the control stick full aft to stall the airplane. The left wing dropped and the airplane turned 90° as it impacted the ground. The engine continued to run until the pilot shut it down and exited the airplane.
An examination of the airplane’s engine, propeller governor, fuel control unit, and fuel pump revealed no anomalies. An engine data recorder showed an exceedance of the N1 upper limit, followed by a decrease in internal turbine temperature, N1, and propeller rpm, consistent with a lower output by the engine.
The data were reviewed by the engine manufacturer, who concluded that the data were consistent with a feathered propeller; however, the reason for the propeller feathering could not be determined based on the available information.
Probable Cause: Loss of propeller thrust for reasons that could not be determined, since examination of the airplane's engine, propeller, and associated accessories revealed no anomalies.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | CEN15LA389 |
Status: | Investigation completed |
Duration: | 3 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
28-Nov-2018 14:43 |
ASN Update Bot |
Added |
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