Accident Beechcraft A36TC Bonanza N361TC,
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ASN Wikibase Occurrence # 219118
 
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Date:Thursday 6 December 2018
Time:12:30 LT
Type:Silhouette image of generic BT36 model; specific model in this crash may look slightly different    
Beechcraft A36TC Bonanza
Owner/operator:Private
Registration: N361TC
MSN: EA-139
Year of manufacture:1980
Total airframe hrs:2813 hours
Engine model:Continental IO-550-B-RA
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Los Banos Municipal Airport (KLSN), Los Banos, CA -   United States of America
Phase: Landing
Nature:Private
Departure airport:San Jose-Reid-Hillview Airport, CA (RHV/KRHV)
Destination airport:Los Banos Municipal Airport, CA (LSN/KLSN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
After almost 1 hour of flight, the pilot turned onto the left base leg of the traffic pattern at the destination airport, where he intended to practice takeoffs and landings. During the turn, the engine began to sputter. The pilot turned toward the runway and tried to maintain clearance from trees located on the outside of the airport perimeter fence; however, the propeller and landing gear impacted the fence. The airplane came to rest upright about 5 ft from the runway edge, resulting in substantial damage.
Postaccident examination of the engine and fuel system revealed no anomalies. The fuel selector handle had been removed, but the rod that rotated the valve remained intact and attached to the unit. The fuel selector was disassembled, and the ring was found located between detents. Based on its position, it may have been positioned between the left- and right-wing tip tanks; however, the position of the fuel selector at the time of the loss of engine power could not be determined. The pilot reported that there were 74 gallons of fuel onboard at the time of departure; however, neither the distribution of the fuel nor the fuel onboard at the time of the accident was determined.
The reason for the partial loss of engine power could not be determined based on the available information.

Probable Cause: A partial loss of engine power for reasons that could not be determined based on the available information.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR19LA039
Status: Investigation completed
Duration: 3 years and 5 months
Download report: Final report

Sources:

NTSB WPR19LA039

https://flightaware.com/live/flight/N361TC

FAA register: https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N361TC%20

Location

Revision history:

Date/timeContributorUpdates
07-Dec-2018 03:53 Geno Added
02-Jul-2022 14:51 ASN Update Bot Updated [Time, Other fatalities, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report]

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