ASN Wikibase Occurrence # 221203
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Date: | Sunday 27 January 2019 |
Time: | 15:14 |
Type: | Piper PA-32RT-300T Turbo Lance II |
Owner/operator: | Stew Industries LLC |
Registration: | N39650 |
MSN: | 32R-7887132 |
Year of manufacture: | 1978 |
Total airframe hrs: | 6000 hours |
Engine model: | Lycoming TIO-540 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Austin Executive Airport (KEDC), Austin, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Austin Executive Airport, TX (KEDC) |
Destination airport: | Taylor, TX (T74) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed with about 40 gallons of fuel on board and completed several flights to local area airports. After about 75 minutes of total flight time, the pilot departed the last airport and had flown a few miles when the engine began running roughly. He stated he switched the fuel selector back and forth between both fuel tank positions, turned the fuel pump on, and advanced the mixture to full rich, but the engine roughness continued. He performed an emergency landing to a road, during which the airplane hit a parked car. The right wing separated from the fuselage, and the airplane flipped upside down.
Nine gallons of fuel were recovered from the left wing tanks, and the inboard right wing tank was found empty, with the right fuel cap secure on the wing. The outboard right wing tank was ruptured and the right wing fuel lines were compromised during impact, but no evidence of fuel from the right wing tanks was found at the scene. The FAA inspector did not arrive to the accident scene until 3 hours after the accident so any fuel that leaked from the tanks would have evaporated. The on-scene examination noted that the fuel selector lever was found in an intermediate position between the left and right tank detents, about 1 to 2 inches past center, more toward the right tank position.
Recovered engine data monitor (EDM) data associated with the accident flight showed a consistent decrease in cylinder head temperatures (CHTs) during the final 3 minutes of the recording, and exhaust gas temperature (EGT) data showed a series of temperature fluctuations during the same time period. The decreasing CHTs and varying EGTs were consistent with a rough-running engine with fluctuating engine speeds.
Postaccident functional engine test runs were performed, and no anomalies were noted with the engine or fuel system. When the fuel system was configured to mimic fuel available in the left tank and no fuel in the right tank, engine roughness and a partial loss of engine power was duplicated through placement of the fuel selector lever to the approximate position as found at the accident scene. The engine roughness can likely be attributed to a mixture of fuel and air in the fuel system.
It was not possible to compute exact fuel usage associated with all the engine operations on the day of the accident due to a lack of information regarding power settings and altitudes flown. However, computations using best economy and best power fuel flow rates for the 94 minutes recorded by the EDM resulted in fuel used of 21.62 gallons for best economy and 37.6 gallons for best power. The flights conducted that day were at best economy and the total flight time was 1.3 hours. The 94 minutes recorded by the EDM was not the flight time. The pilot's operating handbook states the electric fuel pump should be turned on before switching tanks, and, to provide continuity of fuel flow, the selector should be changed to another tank before fuel is exhausted from the tank in use. If signs of fuel starvation occur at any time during flight, fuel exhaustion should be suspected, and the fuel selector should be immediately positioned to a full tank and the electric fuel pump switched to the on position.
Probable Cause: The pilot's fuel mismanagement and his improper use and placement of the fuel selector, contrary to operating procedures, which resulted in a partial loss of engine power due to fuel starvation.
This is a guess by the NTSB of the cause but a key piece of information left out in the initial report. The right wing had holes in fuel tanks caused by the accident. The FAA did not arrive on the scene until 3 hours after the accident, and the NTSB did not check for fuel in the right wing until a month after the accident. There should have been at least 9 gallons of fuel in that tank and would have evaporated before the FAA even arrived.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA076 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/live/flight/N39650 FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=39650%20 Location
Images:
Photo: FAA
Revision history:
Date/time | Contributor | Updates |
27-Jan-2019 23:43 |
Geno |
Added |
09-Aug-2020 07:24 |
ASN Update Bot |
Updated [Time, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ] |
09-Aug-2020 09:51 |
harro |
Updated [Departure airport, Source, Narrative, Photo, Accident report, ] |
02-Oct-2021 14:46 |
sodunlap |
Updated [Phase, Source, Narrative] |
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