ASN Wikibase Occurrence # 222459
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Date: | Wednesday 5 July 2017 |
Time: | 14:40 |
Type: | Piper PA-32-300 Cherokee Six |
Owner/operator: | Private |
Registration: | N112DE |
MSN: | 32-7940044 |
Year of manufacture: | 1979 |
Total airframe hrs: | 6396 hours |
Engine model: | Lycoming IO-540-K1G5 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Rushville, IN -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Fort Wayne Municipal Airport/Baer Field, IN (FWA/KFWA) |
Destination airport: | Jeffersonville-Clark Regional Airport, IN (JVY/KJVY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airline transport pilot and two passengers were on a cross-country flight. While the airplane was descending, the pilot attempted to level off, but the engine did not respond to his throttle input. The pilot decided to divert and began troubleshooting the engine. The pilot could decrease engine power with throttle movement but could not restore engine power with throttle movement. Subsequently, the throttle would not advance past three-fourths of the distance to full throttle application, and the airplane was unable to maintain its altitude. Because the airplane would be unable to reach a nearby airfield, the pilot performed a forced landing to a field, during which the airplane’s firewall was substantially damaged.
Postaccident examination of the airplane found that the throttle control arm was improperly fastened, resulting in throttle arm slippage, which precluded proper control of the engine. It could not be determined if the throttle arm was improperly fastened during the airplane’s last annual inspection, which occurred about 3.5 months before the accident. The airplane had accumulated 12 hours of flight time since the inspection.
Probable Cause: The pilot’s inability to properly control engine power because of an improperly installed throttle control arm, which resulted in a partial loss of engine power and led to a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN17LA271 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
02-Mar-2019 14:46 |
ASN Update Bot |
Added |
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