ASN Wikibase Occurrence # 223988
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Date: | Saturday 19 August 2017 |
Time: | 13:10 |
Type: | Cessna R182 |
Owner/operator: | Private |
Registration: | N9155C |
MSN: | R18200427 |
Year of manufacture: | 1978 |
Total airframe hrs: | 6196 hours |
Engine model: | Lycoming O-540 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Clearwater, FL -
United States of America
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Phase: | |
Nature: | Private |
Departure airport: | Tampa, FL (VDF) |
Destination airport: | Clearwater, FL (CLW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot stated that he performed a preflight inspection of the airplane and did not notice any hydraulic leaks near the landing gear system. After takeoff, he retracted the landing gear and noted that the amber landing gear “UP” indicator had illuminated. While on the downwind leg of the traffic pattern, the pilot attempted to extend the landing gear, but they did not extend completely and lock. He then departed the traffic pattern and performed the landing gear malfunction procedures in the pilot operating handbook to no avail. Next, he performed several maneuvers to lock the landing gear in the down position for about 1 hour but was unsuccessful and chose to return to the airport and perform a gear-up landing. After landing, the pilot tried to maintain directional control of the airplane; it came to rest on the runway and sustained substantial damage to the left horizontal stabilizer.
Postaccident examination of the hydraulic system revealed that there was no hydraulic fluid in the reservoir and that hydraulic fluid was leaking from the rubber landing gear down return line. The line was removed, and a leak was noted. The airframe manufacturer’s service manual indicated that all rubber parts in the landing gear system, which includes the rubber landing gear down return line, should be replaced every 5 years. Examination of the airplane’s maintenance records revealed that there were no maintenance entries related to servicing or replacing that line. Because the landing gear down return line was improperly maintained and was never replaced, it is likely that the line failed and leaked hydraulic fluid, depleting the amount of fluid needed for the landing gear system to maintain hydraulic pressure to extend and lock the main landing gear.
Probable Cause: The improper maintenance of the landing gear system and subsequent failure of the hydraulic landing gear down return line, which resulted in a loss of hydraulic fluid and the pilot’s inability to extend and lock the main landing gear.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | ERA17LA287 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
15-Apr-2019 14:43 |
ASN Update Bot |
Added |
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