ASN Wikibase Occurrence # 223999
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Date: | Friday 18 August 2017 |
Time: | 18:09 |
Type: | Bellanca 7ACA |
Owner/operator: | Private |
Registration: | N9176L |
MSN: | 35-72 |
Year of manufacture: | 1971 |
Total airframe hrs: | 1037 hours |
Engine model: | Continental C85-12F |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fairhope, AL -
United States of America
|
Phase: | |
Nature: | Private |
Departure airport: | Daphne, AL (PVT) |
Destination airport: | Fairhope, AL (CQF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot stated that he had already completed several landings and had just taken off and started a left crosswind turn about 500 ft above ground level when the engine lost total power. He immediately lowered the nose of the airplane, checked the fuel selector position, and applied carburetor heat. The engine restarted, and the pilot began a climb; however, the engine stopped running again, restarted, and then quit a third time. By this time, the pilot-rated passenger had taken control of the airplane and performed a forced landing to a field, which resulted in substantial damage to the fuselage and right wing. Postaccident examination of the airplane revealed that adequate fuel remained in both fuel tanks, and a test run of the engine showed that it ran through its entire power band without interruption. The examination did not reveal any evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation. Although the weather conditions were conducive to the formation of carburetor ice at cruise/glide engine power settings, the airplane was operating at a high power setting; thus, it is unlikely that ice formed in the carburetor during takeoff.
Probable Cause: A total loss of engine power for reasons that could not be determined because postaccident examination and a test run of the engine did not reveal any evidence of mechanical malfunctions or failures that would have precluded normal operation.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | ERA17LA282 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
15-Apr-2019 14:44 |
ASN Update Bot |
Added |
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