ASN Wikibase Occurrence # 224767
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 5 May 2019 |
Time: | 11:17 LT |
Type: | Scheibe SF 25C Falke |
Owner/operator: | Varbergs Flygklubb |
Registration: | SE-USN |
MSN: | 44342 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Varberg/Getterön Airport (ESGV) -
Sweden
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Varberg Airfield (ESGV) |
Destination airport: | Varberg Airfield (ESGV) |
Investigating agency: | SHK |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The intention of the flight was to carry out a shorter flight with take-off and landing at Varberg/Getterön Airport. Aside from the pilot there was one passenger on board.
Take-off proceeded normally up to the point that the aeroplane had become airborne, when the engine suddenly shut down. The pilot attempted to restart the engine. Shortly after this, however, the left wing hit the ground. Based on the available video evidence and information from witnesses, SHK concludes that the aeroplane lost so much speed that it ended up in a stall, resulting in an increasing vertical speed.
The aeroplane suffered substantial damage to both its fuselage and wings. The pilot suffered serious injuries, while the passenger escaped with minor injuries.
During the technical examinations of the engine, it was possible to establish that one of the metal plates that drive the pump diaphragm in the fuel pump had come loose. The investigation of the riveting of the drive plates showed that the flattened rivet head had not been sufficiently expanded. In view of this, SHK has concluded that the engine failure was caused by one of the drive plates having come loose as a result of faulty assembly.
The engine failure occurred despite the engine having recently been at an overhaul. However, the investigation indicates that the fuel pump in question was not approved for installation in the engine. Consequently, SHK determines that a contributing cause of the accident was that the aforementioned non-approved fuel pump was not replaced by the maintenance organisation in conjunction with the engine overhaul and that this was not detected by either the flying club, the technician who reinstalled the engine following the overhaul or by the Swedish Soaring Federation’s airworthiness organisation (SFF CAMO). In summary,
SHK determines that the safety barriers, which aim to ensure that only approved, safe and reliable components are installed in aircraft, have not functioned in this case.
It is SHK’s opinion that the engine failure resulted in a serious accident because the pilot had limited experience, training and mental preparedness to deal with the situation in accordance with the emergency checklist.
Accident investigation:
|
| |
Investigating agency: | SHK |
Report number: | L-53/19 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
https://www.gp.se/nyheter/västsverige/flygplan-kraschade-strax-efter-start-1.14909452
https://www.aftonbladet.se/nyheter/a/vQn7vV/flygplan-i-olycka-vid-flygklubb--tva-till-sjukhus ____________________
http://varbergsflyg.se/motorsegelflyg/tmg-flygplanen/ Media:
Revision history:
Date/time | Contributor | Updates |
05-May-2019 13:16 |
RobertMB |
Added |
05-May-2019 15:58 |
Iceman 29 |
Updated [Time, Source, Embed code] |
22-Jul-2020 14:48 |
harro |
Updated [Location, Nature, Departure airport, Destination airport, Embed code, Narrative, Accident report, ] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation