ASN Wikibase Occurrence # 226001
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Date: | Monday 1 October 2018 |
Time: | 03:30 |
Type: | Cessna 340 |
Owner/operator: | Windy Point Aviation LLC |
Registration: | N89AM |
MSN: | 340-0545 |
Year of manufacture: | 1975 |
Engine model: | Continental TIO-550 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Keokuk, IA -
United States of America
|
Phase: | |
Nature: | Executive |
Departure airport: | Chicago, IL (ORD) |
Destination airport: | Mount Pleasant, IA (MPZ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, while conducting an instrument approach at night in instrument meteorological conditions, about 50 ft above the decision altitude of 921 ft, he mistook building lights for runway lights. He inadvertently touched down the airplane in a soybean field about 3/4 mile short of the runway. He then increased engine power to full, and the airplane climbed "a couple hundred feet." Once he established visual contact with the runway lights, he landed the airplane on the runway without further incident.
The pilot added that the lateral guidance from the localizer was "dead center" but that he could not recall the position of the vertical guidance needle.
The airplane sustained substantial damage to the left wing.
The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
The airport’s automated weather observation station reported that, about 5 minutes after the accident, the wind was from 030° at 3 knots, visibility was 1/2 statute mile with mist, overcast at 200 ft above ground level (agl), temperature 57°F, and dew point 57°F. The pilot reported that the airport ceiling was overcast at 300 ft agl with fog and rain and that visibility was 1 mile.
Probable Cause: The pilot's failure to correctly identify the runway environment during an instrument approach at night in instrument meteorological conditions because he mistook building lights for runway lights, which resulted in landing short of the runway.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA19CA001 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
10-Jun-2019 06:47 |
ASN Update Bot |
Added |
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