ASN Wikibase Occurrence # 228071
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Date: | Friday 9 August 2019 |
Time: | 15:20 LT |
Type: | North American T-28A Trojan |
Owner/operator: | Private |
Registration: | N9862C |
MSN: | 159-239 |
Total airframe hrs: | 2378 hours |
Engine model: | Kaiser R1300-1B |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Ontario Municipal Airport (KONO), Ontario, OR -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Ontario Airport, OR (ONO/KONO) |
Destination airport: | Ontario Airport, OR (ONO/KONO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and one passenger were conducting a flight to test the landing gear. Following a low pass over the runway, the engine lost total power, and the pilot performed a forced landing to a field, during which he was fatally injured, and the passenger sustained serious injuries.
Postaccident examination of the carburetor revealed that, when the throttle arm was placed near the idle position, the internal idle valve was closed, which restricted fuel from flowing through the carburetor at lower power settings and likely resulted in the loss of engine power. It is likely that the pilot reduced the engine power during the low pass to a setting that would have allowed for the idle valve to close completely, thereby restricting the fuel flow. No additional anomalies were noted with the engine or airframe.
The airplane had not flown for about 8 years and had undergone maintenance for the previous 10 months before it first flew 6 days before the accident. One of the maintenance items performed included installation of a new carburetor. The mechanic who performed the annual inspection reported that he assisted in adjusting the idle setting on the carburetor. Whether any additional maintenance was performed on the carburetor before the accident flight could not be determined, and the engine logbook was not available for review.
Probable Cause: A total loss of engine power due to the improperly adjusted carburetor idle valve.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR19FA215 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB WPR19FA215
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=9862C Location
Media:
Revision history:
Date/time | Contributor | Updates |
10-Aug-2019 00:59 |
Geno |
Added |
10-Aug-2019 06:59 |
dfix1 |
Updated [Aircraft type, Total occupants, Phase, Source, Damage, Narrative] |
10-Aug-2019 17:08 |
linbb |
Updated [Aircraft type] |
10-Aug-2019 19:43 |
Captain Adam |
Updated [Aircraft type, Total fatalities, Total occupants, Source, Narrative] |
10-Aug-2019 21:54 |
Iceman 29 |
Updated [Source, Embed code] |
12-Aug-2019 15:05 |
RobertMB |
Updated [Time, Aircraft type, Registration, Cn, Operator, Nature, Source, Embed code] |
01-Jul-2022 19:23 |
ASN Update Bot |
Updated [Time, Cn, Other fatalities, Departure airport, Destination airport, Source, Embed code, Narrative, Category, Accident report] |
02-Jul-2022 07:12 |
harro |
Updated [Cn, Source, Narrative] |
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