ASN Wikibase Occurrence # 228105
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Date: | Friday 9 August 2019 |
Time: | 17:20 LT |
Type: | Cessna 206 |
Owner/operator: | Skinner Leasing LLC |
Registration: | N5152U |
MSN: | 206-0152 |
Year of manufacture: | 1964 |
Total airframe hrs: | 15563 hours |
Engine model: | Continental IO-520-A5B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | E of Rustler Peak, 2 miles SE of Prospect, OR -
United States of America
|
Phase: | Landing |
Nature: | Fire fighting |
Departure airport: | Medford-Rogue Valley International, OR (MFR/KMFR) |
Destination airport: | Medford-Rogue Valley International, OR (MFR/KMFR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:About 2.8 hours into the fire reconnaissance mission flight, the pilot heard a loud bang followed by violent shaking of the airplane. The pilot believed the airplane was at an altitude of about 1,500-2,000 ft. above the ground. The pilot retarded the propeller control to extend his glide distance while he looked for a place to land. The airplane touched down in a swamp and during the landing, the left wing and fuselage were substantially damaged.
A postaccident examination of the engine revealed extensive damage to the no. 1 cylinder, piston, and connecting rod. The no. 1 cylinder valve guide rods broke through the crankcase, and the rear counterweight and counterweight lobe were broken free from the crankshaft. Numerous metal pieces and shavings were noted in the oil pan including: a broken counterweight, crankshaft counterweight attachment, counterweight retainer pin, damaged retainer pin plates, damaged retainer plate spring clips, and engine casing pieces. One of the damaged retainer pin plates displayed a deep groove, the approximate diameter of a counterweight pin.
It is likely that the counterweight retaining pin rotated over time on the counterweight retainer pin plate, causing it to wear down and eventually fail. When the plate failed, the counterweight retainer pin moved from its position and impacted the no. 1 piston rod, causing the counterweight lobe to fracture and the engine to lose power.
Probable Cause: The failure of the counterweight retainer pin plate which resulted in a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR19LA217 |
Status: | Investigation completed |
Duration: | 2 years and 9 months |
Download report: | Final report |
|
Sources:
NTSB WPR19LA217
https://flightaware.com/live/flight/N5152U FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N5152U Location
Revision history:
Date/time | Contributor | Updates |
11-Aug-2019 14:29 |
Aerossurance |
Added |
11-Aug-2019 15:06 |
RobertMB |
Updated [Operator, Nature] |
11-Aug-2019 19:36 |
Geno |
Updated [Operator, Phase, Departure airport, Destination airport, Source] |
01-Jul-2022 19:23 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Source, Damage, Narrative, Category, Accident report] |
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