ASN Wikibase Occurrence # 228979
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Date: | Thursday 12 September 2019 |
Time: | 08:45 LT |
Type: | Infinity Power Parachute |
Owner/operator: | Private |
Registration: | N6035L |
MSN: | IPP2-105 |
Year of manufacture: | 2002 |
Engine model: | Rotax 582 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Henderson County, Eustace, TX -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Eustace, TX |
Destination airport: | Eustace, TX |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Witnesses observed the powered parachute (PPC) flying about 10 to 15 ft above trees and power lines and said the pilot appeared to be in control of the PPC, the parachute canopy appeared 'full,' and there did not appear to be any mechanical issues.
One of the witnesses, who was a neighbor to the pilot, reported observing the PPC fly over his property and then turn south and disappear from his view. He reported it sounded like the pilot tried to apply additional power to the engine and there were two "snapping sounds" followed by the sound of an impact. He responded to the accident site and observed a wire wrapped around the pilot and the cart. None of the witnesses observed the accident occur.
Postaccident examination of the PPC revealed no anomalies that would have precluded normal operation. The PPC had an adequate amount of fuel onboard. Wreckage signatures were consistent with a wire strike. It is likely the pilot failed to maintain clearance from a wire during the low-level flight, which resulted in a wire strike and an impact with terrain.
Medical evidence showed that the pilot's risk of impairment and incapacitation was elevated due to heart disease, prior stroke, and prescription opioid use but did not establish whether he was impaired or incapacitated. There was no operational evidence that the pilot lost control of the PPC or that it was unusual for him to fly so low in the vicinity of hazards. Thus, whether medical factors contributed to the accident could not be determined. The accident is consistent with the pilot failing to see and avoid a power line while flying at a low altitude.
Probable Cause: The pilot's failure to see and avoid a power line. Contributing was the pilot's decision to fly at an altitude too low to avoid obstacles.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA316 |
Status: | Investigation completed |
Duration: | 2 years and 5 months |
Download report: | Final report |
|
Sources:
NTSB CEN19LA316
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N6035L Location
Media:
Revision history:
Date/time | Contributor | Updates |
12-Sep-2019 20:00 |
Captain Adam |
Added |
12-Sep-2019 20:06 |
Captain Adam |
Updated [Registration, Cn, Source, Embed code] |
12-Sep-2019 20:52 |
Geno |
Updated [Time, Source] |
13-Sep-2019 09:26 |
Iceman 29 |
Updated [Embed code] |
01-Jul-2022 17:01 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Embed code, Narrative, Category, Accident report] |
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