ASN Wikibase Occurrence # 230565
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Date: | Thursday 26 July 2018 |
Time: | 21:00 |
Type: | Continental Copters El Tomcat Mk V-A |
Owner/operator: | Scotts Helicopter Service Inc |
Registration: | N9005T |
MSN: | CCI-74-1 |
Year of manufacture: | 1974 |
Total airframe hrs: | 7510 hours |
Engine model: | Lycoming VO-435-A1F |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Le Sueur, MN -
United States of America
|
Phase: | En route |
Nature: | Agricultural |
Departure airport: | Hastings, MN |
Destination airport: | Le Sueur, MN (12Y) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot stated that, during the preflight inspection of the helicopter before the agricultural flight, there were about 23 gallons of fuel onboard, which he determined was sufficient to complete the 45- to 60-minute flight to his destination. The pilot stated that, before departure, the helicopter fuel gauge indicated “close” to 3/4 full. Based on the helicopter's total fuel capacity (41 gallons), a 3/4-fuel quantity indication would have equated to about 30 gallons. About 50 minutes into the flight and 7 miles from the destination airport, the engine lost power. The pilot performed an autorotation to a field, during which the helicopter impacted terrain and sustained substantial damage.
During postaccident examination of the helicopter, no usable fuel was found; however, the fuel gauge indicated a little over a 1/4 tank of fuel remaining. The examination revealed that the fuel transmitter's resistive element was corroded. The fuel transmitter was tested, and the resistive values were uncorrelated to the transmitter's float position. A new fuel transmitter from the operator’s parts department was tested, and the resistive values corresponded to the float position no anomalies were noted. Although the fuel gauge was indicating that a sufficient amount of fuel was onboard for the flight, the pilot should have visually checked the fuel quantity in the tanks before takeoff to ensure that a sufficient amount of fuel was onboard for the flight, which he did not do. His improper preflight fuel planning and his dependence on erroneous fuel gauges led to the subsequent fuel exhaustion and total loss of engine power.
Probable Cause: The pilot's inadequate preflight and in-flight fuel planning, during which he did not visually check the fuel quantity in the fuel tanks and instead relied on the fuel gauges that were showing erroneous fuel quantity indications, which resulted in fuel exhaustion and the subsequent loss of engine power during cruise flight.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | CEN18LA300 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
12-Nov-2019 17:49 |
ASN Update Bot |
Added |
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