ASN Wikibase Occurrence # 232645
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Date: | Wednesday 29 January 2020 |
Time: | 18:10 LT |
Type: | Beechcraft B60 Duke |
Owner/operator: | 7x Oilfield Services Inc |
Registration: | N50JR |
MSN: | P-303 |
Year of manufacture: | 1974 |
Engine model: | Lycoming TIO540 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | S of McMahon-Wrinkle Airport, Big Spring, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Abilene Regional Airport, TX (ABI/KABI) |
Destination airport: | Odessa Schlemeyer Field, TX (KODO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting a cross-country flight at a cruise altitude of 10,500 ft mean sea level when the left engine lost all power. He secured the engine and elected to continue to his destination. Shortly thereafter, the right engine lost all power. After selecting an airport for a forced landing, he overflew the runway and entered the pattern. The pilot stated that on short final, after extending the landing gear, "the plane quit flying and the airspeed went to nothing." The airplane landed 200 to 300 yards short of the runway threshold, resulting in substantial damage to the wings and fuselage.
During a postaccident examination, only tablespoons of fuel were drained from the left tank. Due to the position of the airplane, the right tank could not be drained; however, when power was applied to the airplane, both fuel quantity gauges indicated empty fuel tanks. Neither fuel tank was breached during the accident, and there was no discoloration present on either of the wings or engine nacelles to indicate a fuel leak; therefore, the loss of engine power is consistent with fuel exhaustion.
Probable Cause: A total loss of engine power in both engines due to fuel exhaustion, which resulted in a landing short of the runway.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN20TA071 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB CEN20TA071
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N50JR Location
Revision history:
Date/time | Contributor | Updates |
30-Jan-2020 02:33 |
Geno |
Added |
30-Jan-2020 02:55 |
Geno |
Updated [Source] |
30-Jan-2020 02:58 |
Geno |
Updated [Location, Source] |
30-Jan-2020 16:47 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Operator, Location, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
30-Jan-2020 16:51 |
RobertMB |
Updated [Location] |
13-Jun-2021 17:09 |
aaronwk |
Updated [Time, Departure airport, Destination airport, Source, Narrative] |
08-Jul-2022 11:08 |
ASN Update Bot |
Updated [Time, Other fatalities, Source, Narrative, Category, Accident report] |
21-Sep-2023 09:57 |
Ron Averes |
Updated [[Time, Other fatalities, Source, Narrative, Category, Accident report]] |
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