Serious incident Airbus A340-313 F-GLZU,
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ASN Wikibase Occurrence # 233559
 
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Date:Tuesday 13 March 2012
Time:04:50 UTC
Type:Silhouette image of generic A343 model; specific model in this crash may look slightly different    
Airbus A340-313
Owner/operator:Air France
Registration: F-GLZU
MSN: 377
Year of manufacture:2000
Engine model:CFMI CFM56-5C4
Fatalities:Fatalities: 0 / Occupants:
Aircraft damage: None
Category:Serious incident
Location:near Paris-Charles de Gaulle Airport (CDG/LFPG) -   France
Phase: Approach
Nature:Passenger - Scheduled
Departure airport:Bamako Airport (BKO/GABS)
Destination airport:Paris-Charles de Gaulle Airport (CDG/LFPG)
Investigating agency: BEA
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The crew took off from Bamako, Mali, on 12 March 2012 at 23 h 59 heading for Paris Charles de Gaulle (CDG) Airport. On arrival, the ATIS indicated that the low visibility procedure (LVP) was in force. The crew prepared themselves for a CAT III precision approach.
The aeroplane was stable at FL90 at about 30 NM from the threshold of runway 08R. Autopilot 1 was engaged in HDG and ALT mode. The autothrottle (ATHR) was engaged in SPEED mode. The speed was stable at 250 kt in accordance with the controller’s request. The crew was in contact with CDG approach. They were cleared to intercept localizer 08R.
At 04:40, the controller cleared the crew to descend to FL80 and five seconds later the aeroplane, stable at FL90, passed above the 3° glide path. The crew was then cleared to descend to FL60. They selected an altitude of 6000 ft on the FCU and the autopilot mode changed to OP DES. The autopilot captured the localizer 08R signal (LOC) and then the LOC mode engaged. When the aeroplane descended to 7220 ft, and was 17.5 NM from the threshold, or about 1275 ft above the glide path, the controller requested that a speed of more than 200 kt be maintained. The aeroplane’s speed was about 250 kt. The crew read back and requested to continue the descent. The controller apologised for his omission then cleared the crew to descend to 3000 ft to intercept the 08R ILS.
The crew selected 220 kt and 3000 ft. The OP DES mode remained active. The aeroplane speed and rate of descent decreased which resulted in increasing the deviation from the glide path. The crew extended the airbrakes. When the aeroplane speed reached the target speed of 220 kt, the rate of descent increased again to a value of -1840 ft/min.
At 10 NM from the runway threshold and at an altitude of 5500 ft, the approach controller requested that the crew maintain a speed of more than 160 kt and that they contact the tower. He did not inform the tower controller that the aeroplane was above the glide path. The crew selected a speed of 210 kt then 183 kt and wing slats/flaps configuration 1. Again, the rate of descent decreased and the aeroplane deviated from the 3° glide path.
The crew contacted the tower and indicated that they were 9 NM out. The aeroplane was at an altitude of 4950 ft (1750 ft above the glide path). The controller initially cleared the crew to continue the approach. The latter read back "Cleared to land 08 right...". The controller indicated that he then checked that the CAT III ground services were clear then confirmed clearance to land.
The crew selected slats/flaps configuration 2 and retracted the airbrakes. About one minute later, they re-extended the airbrakes, set the G/S mode using the APPR switch and engaged autopilot 2. The glide deviation displayed on the PFD indicated to the crew that they were approaching the glide path from above. The aeroplane was 4 NM from the runway threshold, at about 3700 ft (that is 2100 ft above the glide path at 3°) and was located in an ILS signal sidelobe.
About 30 seconds later, the crew extended the landing gear. The glide path capture mode (G/S) was activated when the aeroplane was 2 NM from the runway threshold at 2850 ft (that is about 1600 ft above the glide path at 3°). The ATHR changed to SPEED mode. The pitch attitude increased from 1° to 26° in 12 seconds. The PNF stated that he had called out the difference in the pitch attitude when the chevrons appeared. When the aeroplane pitched up, the speed dropped from 163 kt to 130 kt, the vertical speed changed from – 1600 ft/min to + 3300 ft/min. When the pitch attitude reached 26°, the crew disconnected both autopilots and the PF made a pitch down input almost down to the stop. The pitch attitude and vertical speed decreased. The crew retracted the airbrakes. The throttle levers were in the IDLE position. The speed was 143 kt and the ATHR disengaged. About 30 seconds later, autopilot 1 was engaged, the levers were repositioned on the CL setting and the ATHR was activated. The PF explained that he engaged autopilot 1 to perform a go-around on automatic. The LOC and G/S modes were active and the ATHR was in SPEED mode. The speed was 147 kt. The aeroplane was directly above the runway threshold at an altitude of about 2700 ft. The pitch attitude then decreased from 2° to -5° and the aeroplane descended.
The PF stated that he realised that the modes displayed on the FMA were not appropriate. He then disengaged the AP 8 seconds after having activated it and then displayed a pitch attitude of about 6° and placed the throttle levers in the TOGA setting at an altitude of about 2000 ft.
The crew made a second approach and landed without further difficulties.

CONCLUSION
This serious incident was due to:
- Inadequate monitoring of the aeroplane’s flight path by the controller and by the crew during the CAT III precision approach under radar vectoring;
- The crew’s decision to continue the approach after the FAP when the aeroplane was above the glide path.
The following factors contributed to it:
- The absence of visual reference points on the controllers’ radar screen for glide path interception at altitudes lower than 5,000 ft.
- The crew’s use of an unsuitable method to intercept the glide path from above.
- The autopilot’s capture of an ILS signal from a sidelobe, which generated an excessive increase in pitch attitude.
Flight crew and controller fatigue may have contributed to the occurrence of this serious incident.

Accident investigation:
cover
  
Investigating agency: BEA
Report number: 
Status: Investigation completed
Duration:
Download report: Final report

Sources:

https://www.bea.aero/docspa/2012/f-zu120313.en/pdf/f-zu120313.en.pdf

History of this aircraft

Other occurrences involving this aircraft
22 July 2011 F-GLZU Air France 0 North of the Antilles non
23 December 2014 F-GLZU Air France 0 Antananarivo-Ivato Airport (TNR/FMMI) min
Collision with Ground support equipment
11 March 2017 F-GLZU Air France 0 Bogotá-Eldorado Airport (BOG/SKBO) non
Runway excursion
28 November 2017 F-GLZU Air France 0 near Douala unk

Images:


Figure: BEA

Revision history:

Date/timeContributorUpdates
04-Mar-2020 10:42 harro Added
04-Mar-2020 12:34 harro Updated [Narrative, Photo, Accident report, ]

Corrections or additions? ... Edit this accident description

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