ASN Wikibase Occurrence # 234272
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Date: | Sunday 25 August 2019 |
Time: | 09:45 |
Type: | Hughes 269A |
Owner/operator: | Kelley Aviation Consultants Llc |
Registration: | N653CH |
MSN: | 96-0653 |
Year of manufacture: | 1965 |
Engine model: | Lycomiing HIO-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Shamokin, PA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Shamokin, PA (N79) |
Destination airport: | Shamokin, PA (N79) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The helicopter pilot reported that he was being evaluated for a pilot position with a perspective employer, who was an airplane pilot-rated passenger and occupied the right front seat. He was asked to perform an autorotation as part of the evaluation, and while entering the autorotation, he noticed that the rotor and engine needles were split and that the engine tachometer indicated 0 rpm. He believed that the engine had failed. The pilot maintained the rotor rpm in the green and entered a flare about 40 ft above ground level. He attempted to cushion the landing, but the helicopter landed hard. The pilot reported that he could not hear if the engine was running during the flight because he was wearing a noise-canceling headset.
The helicopter sustained substantial damage to the horizontal airframe tube cross-member.
During postaccident examination of the helicopter, the throttle linkage functioned normally. All spark plugs were removed and examined and exhibited indications of normal combustion. A fuel sample was obtained through the sump valve, and no water or particulate contamination was found. No evidence of any preaccident mechanical malfunctions or failures were found with the helicopter that would have precluded normal operation.
Probable Cause: The pilot's improper landing flare during an autorotation, which resulted in a hard landing. Contributing to the accident was a loss of engine power for reasons that could not be determined because postaccident examination revealed no evidence of any preaccident mechanical malfunctions or failures with the helicopter that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA19CA514 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
23-Mar-2020 18:43 |
ASN Update Bot |
Added |
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