ASN Wikibase Occurrence # 235826
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Date: | Thursday 3 October 2002 |
Time: | 14:40 |
Type: | Cirrus SR22 |
Owner/operator: | NS Enterprises, Inc. |
Registration: | N1223S |
MSN: | 0105 |
Year of manufacture: | 2001 |
Total airframe hrs: | 145 hours |
Engine model: | Continental IO-550-N |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lewisville, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Addison, TX (ADS) |
Destination airport: | Dallas, TX (RBD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During cruise flight, the left aileron separated from one attach point, and the pilot executed a forced landing to a field. Prior to the accident flight, the airplane underwent maintenance for two outstanding service bulletins. During compliance with one of the service bulletins, the left aileron would have been removed and reinstalled. The pilot confirmed with the service center personnel that the maintenance on the airplane was completed and then proceeded to preflight the airplane. After departure, the airplane was level at 2,000 feet mean sea level (msl) for approximately one minute, the pilot noticed that the airplane began "pulling" to the left, and the left aileron was separated at one hinge attach point. The pilot then flew the airplane toward an unpopulated area, shutdown the engine, and deployed the aircraft's ballistic parachute system. Subsequently, the airplane descended to the ground with the aid of the parachute canopy and came to rest upright in a field of mesquite trees. Examination of the left aileron and the airframe aileron hinges revealed that the outboard aileron hinge bolt was missing, and no evidence of safety wire noted. According to maintenance manual procedures, the bolt and washer hardware were to be torqued to a measured 20-25 inch pounds, then safety wired to a actuation fitting. After installation, the manual required a verification of proper hinge bolt installation and torque on the outboard hinge.
Probable Cause: The improper reinstallation of the left aileron by maintenance personnel. A contributing factor was the non-suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW03LA005 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20021008X05290&key=1
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
09-May-2020 11:59 |
ASN Update Bot |
Added |
09-May-2020 12:00 |
harro |
Updated [Aircraft type, Cn, Phase, Narrative, Accident report, ] |
09-May-2020 12:00 |
harro |
Updated [Source, Accident report, ] |
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