ASN Wikibase Occurrence # 236811
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Date: | Thursday 7 June 2018 |
Time: | 16:45 |
Type: | Beechcraft A23 |
Owner/operator: | Private |
Registration: | N8775M |
MSN: | M-591 |
Year of manufacture: | 1964 |
Total airframe hrs: | 3580 hours |
Engine model: | Lycoming IO-346-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sedalia, MO -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Cape Girardeau, MO (CGI) |
Destination airport: | Sedalia, MO (DMO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting touch-and-go landings and had landed uneventfully four times. The fifth touchdown was soft; however, the airplane suddenly turned about 90° to the left. The pilot applied right rudder and reduced the throttle to idle. The airplane departed the runway surface, during which the right horizontal stabilizer struck a light post and sustained substantial damage. The pilot reported that the left brake had locked while braking on rollout. A functional check of the braking system and flight controls did not reveal any mechanical malfunctions or failures that would have precluded normal operation; both left and right wheel brake mechanisms functioned properly.
Reported wind conditions about the time of the accident were wind from 230° at 7 knots. However, the pilot indicated that he had checked the local weather about 20 minutes before landing, which reported wind from 100° at 3 knots. Therefore, the crosswind component would have been about 130° opposite, and 4 knots increased, from what the pilot had previously received. The pilot likely lost directional control of the airplane during the landing due to the unexpected wind shift.
Probable Cause: The pilot’s loss of directional control during the landing rollout due to the unexpected wind shift, which resulted in a runway excursion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN18LA220 |
Status: | Investigation completed |
Duration: | 2 years |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
08-Jun-2020 08:39 |
ASN Update Bot |
Added |
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