ASN Wikibase Occurrence # 240421
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Date: | Tuesday 29 May 2018 |
Time: | 19:58 |
Type: | Hughes Aero Corp Predator C |
Owner/operator: | Private |
Registration: | N369SL |
MSN: | PC010853W406 |
Year of manufacture: | 2008 |
Total airframe hrs: | 79 hours |
Engine model: | Rotax 582ULDCDI |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Minor |
Category: | Accident |
Location: | Copemish, MI -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Copemish, MI (PVT) |
Destination airport: | Copemish, MI (PVT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The sport pilot and a passenger departed in a powered-parachute from the pilot's airstrip with calm winds. No anomalies were detected during the preflight inspection. After departure, the powered-parachute would not climb above 8 ft above ground level and was approaching 20-ft-tall trees. The pilot attempted to land between a wire fence and the tree line, and the powered-parachute subsequently impacted the ground and a tree base. The pilot reported that there were no mechanical malfunctions during the flight and stated that the air was "heavier" than expected.
The field elevation at a nearby airport was 634 ft mean sea level (msl), and the calculated density altitude was about 2,821 ft msl. A review of a recent aerial photograph of the pilot's property showed a mowed 600-ft-long runway with a northwest-southeast orientation. At the time of the accident, no runway could be seen on the property because the grass was between 6 and 12 inches tall and appeared unused except for the accident flight.
The unmowed runway and high-density altitude conditions likely affected the powered-parachute's takeoff performance, which resulted in the aircraft being unable to clear the trees near the runway.
Probable Cause: The pilot's improper decision to take off with a passenger in high-density altitude conditions from a runway with tall grass present, which resulted in the powered-parachute's poor takeoff performance and its inability to clear a tree line and led to a subsequent forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN18LA206 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
23-Aug-2020 16:44 |
ASN Update Bot |
Added |
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