ASN Wikibase Occurrence # 245409
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Date: | Saturday 9 April 2016 |
Time: | 18:18 |
Type: | Boeing 737-522 |
Owner/operator: | Aero Contractors Company of Nigeria |
Registration: | 5N-BLG |
MSN: | 25387/2179 |
Year of manufacture: | 1991 |
Fatalities: | Fatalities: 0 / Occupants: 64 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Lagos-Murtala Muhammed International Airport (LOS/DNMM) -
Nigeria
|
Phase: | Landing |
Nature: | Passenger - Scheduled |
Departure airport: | DNPO |
Destination airport: | DNMM |
Investigating agency: | AIB Nigeria |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Boeing 737-500 aircraft, 5N-BLG, owned and operated by Aero Contractors Company of Nigeria operated on a scheduled commercial flight (NIG316) from Port Harcourt to Lagos on an Instrument Flight Rules (IFR) flight plan. The aircraft touched down on runway 18R and veered right of the centreline into the grass verge.
Prevailing weather information reported rain overhead the station with a visibility of 3,000 m. During ILS approach on runway 18L, at an altitude of about 500 ft, the crew executed a missed approach due strong cross wind. The crew thereafter requested for runway 18R with ATC weather information reporting wind at 090°/15 kt with a visibility of 3,000 m in moderate rain.
The crew stated that the second approach was stable till throttles were closed at 10 ft, for landing. On touchdown, with increase in intensity of rain accompanied with reduced visibility, the aircraft touched down right of the runway centreline and veered into the grass verge. The Captain took control of the aircraft and brought it back to the runway.
The aircraft was taxied to the apron and parked at A6 parking bay. Engines were shut down and all 64 persons onboard the aircraft, including five crew members disembarked with no injuries.
Instrument Meteorological Conditions (IMC) prevailed at the time of the incident. The incident occurred after sunset.
The investigation identified the following:
Causal Factor:
Excessive rudder application by the crew after touchdown.
Contributory Factors:
i. Reduced visibility due heavy rain on touchdown.
ii. The decision to continue approach in an unfavourable weather condition with crosswind component of 090°/15kt.
Accident investigation:
|
| |
Investigating agency: | AIB Nigeria |
Report number: | |
Status: | Investigation completed |
Duration: | 4 years and 8 months |
Download report: | Final report |
|
Sources:
AIB Nigeria
Revision history:
Date/time | Contributor | Updates |
07-Dec-2020 16:08 |
harro |
Added |
07-Dec-2020 16:09 |
harro |
Updated [Narrative] |
07-Dec-2020 16:12 |
harro |
Updated [Narrative] |
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