ASN Wikibase Occurrence # 247329
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Date: | Sunday 31 January 2021 |
Time: | 11:44 LT |
Type: | Cessna T182T Turbo Skylane |
Owner/operator: | Morey's West Coast Adventures, Inc |
Registration: | N291FR |
MSN: | T18209082 |
Year of manufacture: | 2012 |
Total airframe hrs: | 1787 hours |
Engine model: | Lycoming TIO-540-AK1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Lake Earl, NE of Crescent City, CA -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | Medford-Rogue Valley International, OR (MFR/KMFR) |
Destination airport: | Crescent City-McNamara Field, CA (CEC/KCEC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor noticed a flashing red turbine inlet temperature (TIT) warning light during the flight. He enrichened the fuel mixture, which returned the TIT to normal. Shortly after, the engine began to run rough. The flight instructor switched to the left magneto and the engine lost power. He then switched to the right magneto and the engine continued to run rough. He switched back to both magnetos and the engine continued to run rough. The flight instructor then adjusted the mixture and turned on the auxiliary fuel pump. Despite his actions, he was unable to get the engine to operate at a power setting sufficient to maintain altitude. The flight instructor located an open field and initiated a forced landing. The airplane landed in marshland and nosed over during the landing.
The postaccident examination of the engine revealed excessive gap on all sparkplugs and two of the sparkplug electrodes were fouled. The magnetos would not produce spark and had corrosion on their internal components. It was also noted that the pressurized magnetos did not have a moisture trap or filter installed.
The magnetos were sent to a facility for further examination, which revealed deformities on both magneto point assembly contact areas and the failure of both magneto capacitors during testing. The failure of the capacitors likely resulted in the deformities on the points surface contact areas resulting in the magnetos not producing sufficient spark for normal operation.
Probable Cause: The partial loss of engine power due to the failure of both magneto capacitors.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR21LA098 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB WPR21LA098
FAA register:
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N291FR https://flightaware.com/live/flight/N291FR/history/20210131/1830Z/KMFR/KCEC Location
Revision history:
Date/time | Contributor | Updates |
01-Feb-2021 06:44 |
Geno |
Added |
03-Feb-2021 19:52 |
RobertMB |
Updated [Location, Phase, Source] |
09-Jul-2021 19:24 |
aaronwk |
Updated [Time, Nature, Source, Narrative, Category] |
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