Accident Hughes OH-6A Cayuse N6639R,
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ASN Wikibase Occurrence # 247567
 
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Date:Friday 5 February 2021
Time:14:00 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes OH-6A Cayuse
Owner/operator:U.S. Department of Agriculture APHIS
Registration: N6639R
MSN: 66-078784
Total airframe hrs:14627 hours
Engine model:Alison 250-C20B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:between Horseshoe Bend and Gardena, Boise County, ID -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Nampa-KMAN, ID (MAN/KMAN)
Destination airport:Caldwell Industrial Airport, ID (KEUL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While conducting wildlife damage management operations at low altitude over hilly terrain, the pilot of the helicopter noted a loss of main rotor rpm. To regain main rotor rpm, he reduced the engine power demand by descending into a draw; however, the helicopter impacted terrain, rolled over, and came to rest on its left side. Two days before the accident flight, the pilot experienced a similar loss of main rotor rpm; however, he was able to safely land the helicopter. The pilot was unable to replicate the loss of main rotor rpm and continued the flight. The pilot believed that the event was an isolated anomaly and did not notify maintenance personnel.
Postaccident examination of the helicopter revealed an air leak located in the fuel cell outlet valve near the firewall. Subsequent examination of the fuel cell outlet valve revealed circumferential scratch marks around the barrel of the pipe. Damage due to cross-threading was observed on the first two threads. When the O-ring was removed, metal chips were located embedded throughout the O-ring. A review of the maintenance records indicated that the fuel system components were inspected during the 100-hour inspection, along with correspondence from the maintenance facility that a vacuum check of the fuel system was conducted during that inspection, with no anomalies noted. No entries were found in the maintenance records of any work done to the fuel outlet valve. The approved maintenance manual for the helicopter contained multiple warnings that air in the fuel system will cause a power reduction or flame out. It could not be determined when, or how, the fuel cell outlet valve developed a leak.

Probable Cause: A partial loss of engine power due to a leak in the fuel cell outlet valve.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR21LA107
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB WPR21LA107
FAA register: https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?nNumberTxt=6639R

https://flightaware.com/live/flight/N6639R


Location

Revision history:

Date/timeContributorUpdates
07-Feb-2021 00:56 Captain Adam Added
07-Feb-2021 01:35 Geno Updated [Time, Location, Source]
09-Feb-2021 02:59 Geno Updated [Time, Aircraft type, Registration, Cn, Phase, Nature, Departure airport, Source, Narrative]
11-Feb-2021 08:26 RobertMB Updated [Aircraft type, Cn, Source, Narrative]
11-Feb-2021 12:34 Aerossurance Updated [Operator, Location, Nature, Source, Narrative]
26-Sep-2022 19:03 ASN Update Bot Updated [Time, Cn, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report]
26-Sep-2022 19:11 harro Updated [Operator, Source, Narrative]
12-Nov-2022 02:15 Ron Averes Updated [Operator]

Corrections or additions? ... Edit this accident description

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