ASN Wikibase Occurrence # 248723
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Date: | Thursday 11 March 2021 |
Time: | 20:53 LT |
Type: | Cessna 421B Golden Eagle |
Owner/operator: | Duotech Services Inc. |
Registration: | N80056 |
MSN: | 421B-0654 |
Year of manufacture: | 1974 |
Total airframe hrs: | 3406 hours |
Engine model: | Continental GTSSIO520H |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Franklin-Macon County Airport, NC (1A5) -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Franklin-Macon County Airport, NC (1A5) |
Destination airport: | Franklin-Macon County Airport, NC (1A5) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, during the takeoff roll from the 5,000-ft-long runway, after reaching an airspeed of 90 knots, the airplane's acceleration slowed. The airplane reached a maximum airspeed of about 92 knots, which was below the planned rotation speed of 100 knots. The pilot elected to abort the takeoff with about 1,500 ft of remaining runway. He reduced the power to idle and initiated maximum braking. The pilot stated that he did not sense the airplane slowing down but observed tire marks on the runway postaccident that were consistent with braking. The airplane continued off the end of the runway and collided with a fence before coming to a stop. All of the occupants exited the airplane safely, and a post-crash fire ensued.
Examination of the runway revealed tire skid marks that began 1,200 ft from the runway end and continued into the grass leading to the airplane. An examination of the airplane revealed that the entire cockpit and cabin areas were destroyed by fire. The engines did not display evidence of a catastrophic failure but were otherwise unable to be examined in more detail due to the degree of fire damage. The parking brake control was found in the off position. All hydraulic brake lines were destroyed by fire, and the main landing gear sustained fire and impact damage. Although the tire marks on the runway indicated that some braking action took place, the extensive fire damage precluded a detailed examination of the braking system, and there was insufficient evidence to determine the reason for the runway excursion.
Probable Cause: The reason for this accident could not be determined based on the available information.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA21LA152 |
Status: | Investigation completed |
Duration: | 1 year and 11 months |
Download report: | Final report |
|
Sources:
NTSB ERA21LA152
FAA register:
https://registry.faa.gov/aircraftinquiry/Search/NNumberResult https://flightaware.com/live/flight/N80056/history/20210310/1901Z Location
Revision history:
Date/time | Contributor | Updates |
11-Mar-2021 23:49 |
Geno |
Added |
12-Mar-2021 02:37 |
RobertMB |
Updated [Source, Narrative] |
13-Mar-2021 18:23 |
Airwork737 |
Updated [Embed code] |
02-Apr-2021 17:42 |
aaronwk |
Updated [Time, Total occupants, Nature, Destination airport, Source, Narrative] |
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