ASN Wikibase Occurrence # 24920
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 14 April 2003 |
Time: | 11:40 |
Type: | Aero Commander 500S Shrike Commander |
Owner/operator: | Private |
Registration: | N19WL |
MSN: | 3160 |
Year of manufacture: | 1973 |
Total airframe hrs: | 11617 hours |
Engine model: | Lycoming IO-540-E1B5 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Mount Pleasant -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | Mount Pleasant, SC (8S5) |
Destination airport: | Mount Pleasant, SC (8S5) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, he requested the refueler to top off his fuel tanks with "100 low lead fuel". After refueling, the pilot performed a preflight including taking fuel samples from under the wings, draining the rear fuel drain, and checking the fuel cap for security. The engine start, run-up, and taxi were uneventful. The airplane departed runway 17 and was in a positive rate of climb. At approximately 200 feet AGL the airplane began to lose power. Shortly after the pilot ensured that the throttle, propeller, and mixture controls were in the full forward position, the airplane lost power in both engines. The pilot executed an emergency off field landing. Examination of the wreckage revealed that the left wing had broken off and the aft cabin area was crushed. According to the refueler, he stated that he mistakenly used the Jet-A fuel truck instead of the AVGAS 100 low lead truck, and pumped 58 gallons of Jet-A into the airplane. Examination of the fuel samples taken from both engines revealed the left and right engine contained 70 percent of jet A fuel.
Probable Cause: The improper refueling of the airplane by airport personnel with the incorrect fuel grade that resulted in a total loss in engine power on both engines during initial climb. A factor was the inadequate preflight inspection by the pilot in command.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL03TA078 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20030416X00520&key=1 Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Dec-2017 18:32 |
ASN Update Bot |
Updated [Cn, Operator, Nature, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation