ASN Wikibase Occurrence # 260227
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 13 May 2021 |
Time: | 11:17 LT |
Type: | Beechcraft B24R Sierra 200 |
Owner/operator: | Private |
Registration: | N9199S |
MSN: | MC-371 |
Year of manufacture: | 1975 |
Total airframe hrs: | 3843 hours |
Engine model: | Lycoming IO360-A1B6 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | New Lenox, SW of Lockport-Lewis Lockport Airport (LOT/KLOT), IL -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Lockport-Lewis Lockport Airport, IL (LOT/KLOT) |
Destination airport: | Indianapolis-Eagle Creek Airpark, IN (KEYE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot fueled the airplane using containers kept in the flying club hangar. Unknown to the pilot, one of the containers contained water, which he added to the left fuel tank. He noted that no water was observed when the fuel tanks were sumped as part of the preflight inspection; although, there was likely insufficient time for the water to settle out. The engine run-up, takeoff, and initial climb were conducted with the right fuel tank selected and were routine. However, when the pilot changed to the left fuel tank during the climb, the engine lost power. He executed a forced landing to an interstate highway.
About 2-1/2 gallons of water were drained from the left fuel tank following the accident. No water was detected in the right fuel tank. No anomalies with respect to the engine assembly or the airframe fuel system were observed.
An individual associated with the flying club reported that he was cleaning an airplane in the hangar the day before the accident. He had used a fuel container to get water and marked it, 'water for cleaning.' At the end of the day, he left the container next to the airplane with the intention of continuing the next day. There were 2 to 3 gallons of water in the container at the time.
Probable Cause: The total loss of engine power due to fuel contamination as a result of the pilot's improper fueling of the airplane.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN21LA219 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB CEN21LA219
https://flightaware.com/live/flight/N9199S Location
Revision history:
Date/time | Contributor | Updates |
13-May-2021 17:13 |
Captain Adam |
Added |
13-May-2021 20:17 |
Geno |
Updated [Time, Location, Source] |
21-Aug-2022 19:07 |
ASN Update Bot |
Updated [Time, Total occupants, Other fatalities, Destination airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation