ASN Wikibase Occurrence # 26120
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Date: | Wednesday 13 March 2002 |
Time: | 19:40 |
Type: | Beechcraft E90 King Air |
Owner/operator: | Regent Air, Inc. |
Registration: | N948CC |
MSN: | LW-236 |
Year of manufacture: | 1977 |
Total airframe hrs: | 8773 hours |
Engine model: | Pratt & Whitney PT6A-28 |
Fatalities: | Fatalities: 0 / Occupants: 6 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Reno, NV -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | Durango, CO (DRO) |
Destination airport: | Reno, CA (RNO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During an instrument approach, upon descending to the prescribed minimum descent altitude, about 1/2 mile from the missed approach point, the pilot failed to maintain flying airspeed. The airplane stalled, rolled left, and in an uncontrolled descent collided with a commercial building 0.96 nm from the runway's displaced threshold. The accident occurred during the return portion of a round trip flight, while on final approach to the pilot's alternate airport due to a weather-induced diversion. Moderate intensity snow showers and freezing fog existed. During the initial approach, the reported visibility was 1 1/2 miles. About the time the pilot passed the final approach fix, the visibility decreased to 1/2 mile, but the pilot was not informed of the decrease below his 1-mile minimum requirement. The pilot had maintained the recommended 140-knot approach speed in the icing conditions until about 3 1/2 miles from the runway. Thereafter, the airplane's speed gradually decreased until reaching about 75 knots. After the airplane started vibrating, the pilot increased engine power, but his action was not timely enough to avert stalling. Company mechanics maintained the airplane. On previous occasions overheat conditions had occurred wherein the environmental ducting melted and heat was conducted to the adjacent pneumatic tube that provides deice air to the empennage boots. During the accident investigation, the deice tube was found completely melted closed, thus rendering all of the empennage deice boots dysfunctional.
Probable Cause: The pilot's inadequate approach airspeed for the existing adverse meteorological conditions followed by his delayed remedial action to avert stalling and subsequent loss of airplane control. Contributing factors were the pilot's reduced visibility due to the inclement weather and the icing conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX02FA108 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20020403X00453&key=1 Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
28-Jan-2013 23:55 |
wf |
Updated [Cn, Phase, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Dec-2017 15:51 |
ASN Update Bot |
Updated [Operator, Departure airport, Destination airport, Source, Narrative] |
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