ASN Wikibase Occurrence # 263630
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Date: | Friday 4 June 2021 |
Time: | 17:30 LT |
Type: | Piper PA-28-140 Cherokee |
Owner/operator: | MWH Consulting |
Registration: | N8208N |
MSN: | 28-25411 |
Year of manufacture: | 1969 |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Justin-Flying S Farm Airport, TX (3TX2) -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Justin-Flying S Farm Airport, TX (3TX2) |
Destination airport: | Justin-Flying S Farm Airport, TX (3TX2) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that he and a passenger were to conduct three takeoffs and landings in preparation for the airplane to be sold. Immediately after the third takeoff, when the airplane was about 45 ft above ground level, the engine experienced a loss of power. The left wing dropped, and the airplane descended into trees. The left wing separated at the wing root during the accident sequence and the airplane came to rest suspended in the trees. The pilot stated that the airplane had not received an annual inspection in about 7 years and had not been flown much in recent years.
A basic postaccident examination found that the airplane sustained substantial damage to the wings and fuselage. There was a smell of fuel at the accident site. The left fuel tank was intact and contained about 1 gallon of fuel. The right fuel tank was breached and did not contain any fuel. The fuel selector was positioned to the right tank.
The pilot was contacted via email and phone on multiple occasions but did not submit the National Transportation Safety Board (NTSB) Pilot/Operator Aircraft Accident/Incident Report Form 6120.1. The airplane was moved to private property and the NTSB was unable to examine the wreckage.
Based on the limited available evidence, the reason for the loss of engine power could not be determined.
Probable Cause: The loss of engine power for undetermined reasons based upon the available information.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN21LA249 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB CEN21LA249
FAA register:
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N8208N Location
Revision history:
Date/time | Contributor | Updates |
05-Jun-2021 01:46 |
Geno |
Added |
05-Jun-2021 02:20 |
RobertMB |
Updated [Time, Aircraft type, Nature, Source, Narrative] |
05-Jun-2021 02:21 |
RobertMB |
Updated [Damage, Narrative] |
07-Jun-2021 15:41 |
RobertMB |
Updated [Registration, Cn, Operator, Source, Narrative] |
07-Jun-2021 21:31 |
Captain Adam |
Updated [Departure airport, Destination airport, Narrative] |
09-Jun-2021 07:46 |
Anon. |
Updated [Source, Damage, Narrative] |
26-Sep-2022 18:58 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report] |
26-Sep-2022 19:00 |
harro |
Updated [Operator, Location, Departure airport, Destination airport, Source, Narrative] |
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