ASN Wikibase Occurrence # 264239
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Date: | Saturday 14 March 2020 |
Time: | 12:15 LT |
Type: | Cessna 182P Skylane |
Owner/operator: | Private |
Registration: | N20847 |
MSN: | 18261254 |
Year of manufacture: | 1972 |
Total airframe hrs: | 10912 hours |
Engine model: | Continental IO-520-D (116 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lumberton, MO -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Columbia, MS (0R0) |
Destination airport: | Picayune-Picayune Municipal Airport, MS (KMJD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and passenger were conducting a personal flight when the engine experienced a partial loss of power. The pilot was unable to maintain altitude and made a forced landing to a road. During the forced landing, while turning right to stay on the road, the airplane ground looped and collided with trees, sustaining substantial damage.
Examination of the engine revealed that a portion of the No. 1 cylinder valve head was fractured due to the inward propagation of a radial rim fracture, and the initiation and propagation of a chordal fracture in the filet area perpendicular to the axis of the stem. The initial crack developed at the rim and propagated inward toward the center of the valve head as a radial rim crack. When the crack front reached the fillet region of the head, a second crack initiated and propagated in fatigue as a chordal fracture. A final overstress fracture occurred near the rim. This type of failure is likely due to cyclic uneven expansion and contraction stress cracks that propagate inward, as a result of inadequate valve seating.
The engine maintenance records showed that a repaired No. 1 cylinder was installed on May 9, 2014. The partial maintenance release stated that the cylinder repair process included refaced valves and three angle cut valve seats. There were no other entries related to the No. 1 cylinder. The engine had accumulated about 598 hours since the cylinder was installed. Annual inspections were completed every year after this cylinder installation.
Probable Cause: The failure of the No. 1 cylinder intake valve due to inadequate valve seating.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN20LA123 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB CEN20LA123
Location
Revision history:
Date/time | Contributor | Updates |
20-Jun-2021 05:51 |
aaronwk |
Added |
01-Jul-2022 14:22 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report] |
01-Jul-2022 14:33 |
harro |
Updated [Destination airport, Narrative] |
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