ASN Wikibase Occurrence # 266701
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 11 August 2021 |
Time: | 15:57 |
Type: | Air Tractor AT-802F Fire Boss |
Owner/operator: | Forest Protection Limited |
Registration: | C-GJJX |
MSN: | 802-0121 |
Year of manufacture: | 2002 |
Engine model: | PWC PT6A-67AG |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | near Mount Carleton, New Brunswick, Northumberland County -
Canada
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Fire fighting |
Departure airport: | Miramichi Airport, NB (YCH/CYCH) |
Destination airport: | Miramichi Airport, NB (YCH/CYCH) |
Investigating agency: | TSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:An Air Tractor AT-802 operated by Forest Protection Limited, operating as Tanker 624, was conducting forest fire fighting operations out of the Miramichi (CYCH), NB Airport with 1 crew member on board. At approximately 1557 ADT, while conducting the fourth bombing run of the day, the aircraft impacted the hillside of a heavily wooded area of northern New Brunswick. The pilot sustained minor injuries and was able to walk to a nearby road, where he was taken by helicopter and ambulance to a local hospital.
There was no post accident fire, however, the aircraft was destroyed.
Findings as to causes and contributing factors
- During the aborted drop, the power was increased to 58% of the available power, and the flaps were retracted from 30° to 20°. Due to the pilot’s high workload and divided attention, these settings went unnoticed.
- The selected power setting, combined with the flap setting, contributed to a reduced airspeed as the aircraft entered a slow climb to avoid rising terrain.
- As the aircraft approached rising terrain, the low altitude and tailwind resulted in the pilot perceiving that the airspeed was sufficient when, in fact, it was decreasing.
- As the aircraft approached the stall, the stall warning horn sounded. Because the pilot perceived the aircraft’s speed to be sufficient, the pilot identified this audio tone to be the sound that warns of an over-torque condition, and as a result, he decreased power.
- As a result of the decreased power, the aircraft decelerated further, stalled, and entered an incipient spin at an altitude too low to permit recovery.
Accident investigation:
|
| |
Investigating agency: | TSB |
Report number: | A21A0024 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
https://www.cbc.ca/news/canada/new-brunswick/water-bomber-pilot-safe-after-crash-1.6138888 TSB
Location
Images:
Photo: TSB
Revision history:
Date/time | Contributor | Updates |
12-Aug-2021 20:37 |
Geno |
Added |
13-Aug-2021 09:29 |
harro |
Updated [Operator, Damage] |
14-Aug-2021 06:01 |
Anon. |
Updated [Narrative, Category] |
07-Jan-2022 14:24 |
harro |
Updated [Time, Registration, Source, Damage, Narrative] |
07-Jan-2022 14:24 |
harro |
Updated [Cn] |
10-Aug-2022 13:10 |
harro |
Updated [Departure airport, Destination airport, Narrative, Accident report] |
10-Aug-2022 13:12 |
harro |
Updated [Narrative, Photo] |
22-Jul-2023 00:38 |
Ron Averes |
Updated [[Narrative, Photo]] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation