ASN Wikibase Occurrence # 266907
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Date: | Monday 16 August 2021 |
Time: | 14:15 LT |
Type: | Europa XS Trigear |
Owner/operator: | Private |
Registration: | N133AC |
MSN: | A060 |
Year of manufacture: | 1999 |
Total airframe hrs: | 1099 hours |
Engine model: | Rotax 914 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hanksville, UT -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Halls Crossing, UT (U96) |
Destination airport: | Manti, MT (41U) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot replaced lost fluid in the airplane engine's cooling system with water and after a successful ground run, the pilot departed. During a “stair-stepped' climbout, the engine's cylinder head temperature (CHT) increased into the red arc of the CHT gauge (the maximum admissible cylinder head temperature of 180°C [356°F]). The pilot immediately reduced the throttle setting to ide and elected to conduct a forced landing. The airplane sustained substantial damage to the wings and fuselage after impacting rough terrain during the landing.
Postaccident examination of the cooling system revealed that system components were secured and void of all fluid. Testing of the accident radiator cap revealed that it was a non-original equipment manufactured (OEM) part by a third-party vendor and that the pressure relief valve opened and released air pressure about 0.2 bar (3 psi), less than the manufacturer's recommended coolant system maximum pressure value of 1.2 bar (18 psi).
It is likely that the lack of pressure created by the non-OEM radiator cap reduced the coolant boiling point and system pressure. The pressure reduction and lowering of the boiling point would have allowed the coolant to evaporate, leading to a loss of coolant in the system and the engine's exceedance of the maximum admissible cylinder head temperature of 180°C (356°F).
Probable Cause: The pilot's installation of a non-original equipment manufactured radiator cap, which resulted in the loss of coolant and the engine's exceedance of the maximum admissible cylinder head temperature. Contributing to the accident was the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR21LA325 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB WPR21LA325
https://flightaware.com/live/flight/N133AC/history/20210816/1741Z/KAEG/L%2036.75929%20-109.39267 Location
Revision history:
Date/time | Contributor | Updates |
19-Aug-2021 01:23 |
Captain Adam |
Added |
22-Aug-2021 17:15 |
harro |
Updated [Aircraft type] |
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