ASN Wikibase Occurrence # 269267
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Date: | Saturday 30 October 2021 |
Time: | 18:10 LT |
Type: | Cessna 177 Cardinal |
Owner/operator: | private |
Registration: | N29615 |
MSN: | 17700993 |
Year of manufacture: | 1968 |
Total airframe hrs: | 2262 hours |
Engine model: | Lycoming O-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Parker County Airport (WEA/KWEA), Weatherford, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Guthrie Airport, OK (GOK/KGOK) |
Destination airport: | Hudson Oaks, TX |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a personal flight, the pilot was descending the airplane for landing and added throttle, but the engine did not respond. The pilot decided to make a forced landing, during which the airplane collided with power lines and terrain, resulting in substantial damage to the airplane.
Postaccident examination of the airplane and engine found damage in the engine area that precluded documentation of the throttle cable's full range of travel. Examination of the accident site found no evidence of fuel in the tanks, but fuel did not appear to have leaked from the tanks. The pilot reported that the airplane should have contained at least 10 gallons of fuel. Thus, the pilot's fuel calculations could have been incorrect, resulting in fuel exhaustion. In addition, the airplane was operating in an area conducive for the formation of serious icing at glide power. However, the pilot stated that he applied carburetor heat and enrichened the mixture when he began descending.
The postaccident airplane and engine examination revealed no preimpact anomalies that would have precluded normal operation. As a result, and based on the available evidence, the reason for the partial loss of engine power was most likely the result of fuel exhaustion.
Probable Cause: The partial loss of engine power due to fuel exhaustion. Contributing was the pilot's improper fuel planning.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN22LA036 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB CEN22LA036
FAA register:
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=104HJ https://flightaware.com/live/flight/N29615/history/20211030/2211Z/0OK6/KWEA Location
Revision history:
Date/time | Contributor | Updates |
31-Oct-2021 03:30 |
Geno |
Added |
31-Oct-2021 03:43 |
Geno |
Updated [Time, Registration, Cn, Operator, Departure airport, Destination airport, Source, Narrative] |
31-Oct-2021 03:44 |
Geno |
Updated [Destination airport] |
31-Oct-2021 05:16 |
RobertMB |
Updated [Registration, Phase, Nature, Source, Narrative] |
31-Oct-2021 05:18 |
RobertMB |
Updated [Aircraft type] |
11-Jun-2023 08:12 |
ASN Update Bot |
Updated [[Aircraft type]] |
11-Jun-2023 08:17 |
harro |
Updated [[[Aircraft type]]] |
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