ASN Wikibase Occurrence # 278551
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 8 September 2021 |
Time: | 16:45 LT |
Type: | Enstrom F-28 |
Owner/operator: | private |
Registration: | N51789 |
MSN: | 454-2 |
Year of manufacture: | 1978 |
Total airframe hrs: | 3802 hours |
Engine model: | Lycoming HIO-360 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Toughkenamon, Pennsylvania -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Toughkenamon, PA |
Destination airport: | Toughkenamon, PA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot performed a straight in approach to runway 24 and then entered an out-of-ground-effect hover at 30 to 40 ft above ground level. He made a right turn to hover taxi to the fueling area. At that time, he noticed that the rotor rpm was low, and he attempted to increase it; however, the helicopter spun right, descended and impacted a grass area near a taxiway. The recorded wind at the airport about the time of the accident was variable at 4 knots, gusting to 10 knots. The pilot reported 10 to 12 knot gusts from the east at the time of the accident and previous and subsequent weather recordings indicated wind gusts from the south. Examination of the wreckage by a Federal Aviation Administration inspector revealed substantial damage to the lower right fuselage. The examination did not reveal any preimpact mechanical malfunctions, nor did the pilot report any. It is likely that the helicopter was in an out-of-ground effect hover with a direct or quartering tailwind, which resulted in a loss of tail rotor effectiveness.
Probable Cause: The pilot's failure to maintain control of the helicopter during an out-of-ground effect hover in a gusty wind, due to loss of tail rotor effectiveness.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA21LA357 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB ERA21LA357
Location
Revision history:
Date/time | Contributor | Updates |
31-May-2022 17:22 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation