ASN Wikibase Occurrence # 278711
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Date: | Wednesday 7 July 2021 |
Time: | 09:31 LT |
Type: | Piper PA-28-140 |
Owner/operator: | Bethany Aviation |
Registration: | N91W |
MSN: | 28-25441 |
Year of manufacture: | 1969 |
Total airframe hrs: | 7037 hours |
Engine model: | Lycoming O-320-E3D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Greensboro, North Carolina -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Greensboro/High Point-Piedmont Triad International Airport, NC (GSO/KGSO) |
Destination airport: | Greensboro, NC |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The student pilot was approaching to land at his home airport on a solo flight. The wind was almost directly down the runway at 6 knots. After he turned onto the base leg of the traffic pattern, air traffic control (ATC) inquired if he had turned base. He informed them he had and needed to immediately turn on the final. ATC then asked an airplane to hold position. His approach angle was normal, he was on the centerline, and his airspeed was about 85 mph. As he crossed the threshold of the runway, he reduced the throttle to idle, and the airplane touched down firmly, but did not bounce. When the nosewheel contacted the runway pavement, the airplane began shaking and the airplane began heading towards the right side of the runway. The student pilot attempted to correct, but his corrections started a series of oscillations which grew in amplitude. The airplane then entered the grass next to the runway and he let the airplane continue along its path of travel for fear of flipping the airplane over. The airplane then encountered a drainage ditch and came to rest on the other side of it. The airplane was substantially damaged. The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause: The student pilot's improper flare which resulted in abnormal ground contact and loss of control.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA21LA285 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB ERA21LA285
Location
Revision history:
Date/time | Contributor | Updates |
02-Jun-2022 19:28 |
ASN Update Bot |
Added |
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