ASN Wikibase Occurrence # 279960
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 20 September 2020 |
Time: | 11:45 LT |
Type: | Zenith CH 750 |
Owner/operator: | |
Registration: | N210WP |
MSN: | 75-8690 |
Year of manufacture: | 2014 |
Total airframe hrs: | 74 hours |
Engine model: | Viking Aircraft Engines 110 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Montrose, Missouri -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Goldsworthy Airport, WA (GLY) |
Destination airport: | Parsons, MO (0KS8) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot of the experimental, amateur-built airplane was en route to the destination airport when the engine momentarily lost power. The pilot immediately selected the alternate fuel pump and engine control unit (ECU), and the engine regained power. About 5 minutes later, the engine lost total power, and the pilot attempted to restart the engine. The engine restart was unsuccessful, and the pilot performed a forced landing to a field, during which the airplane nosed over and came to rest inverted, resulting in substantial damage to the left wing and rudder.
Postaccident examination of the airplane revealed that the main fuse block was discolored and exhibited internal thermal damage. An automotive blade-type fuse that connected to both primary and secondary fuel pumps and primary and backup ECUs displayed arcing signatures and had failed. According to the engine manufacturer, the primary and secondary ECUs should have been wired directly to the main bus and should not have contained a fuse. The improper installation of the airplane's electrical system resulted in an overloaded electrical system for the installed fuse. After bypassing the failed electrical system, an engine test run was performed. The engine started and operated normally with no mechanical issues noted.
Probable Cause: A total loss of engine power due to an electrical overload in the engine control unit wiring system; the electrical overload occurred as a result of improper installation by the airplane builder.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN20LA412 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB CEN20LA412
Location
Revision history:
Date/time | Contributor | Updates |
03-Jul-2022 07:24 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation