ASN Wikibase Occurrence # 280496
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Date: | Monday 18 July 2022 |
Time: | 08:04 |
Type: | Van’s RV-10 |
Owner/operator: | Private |
Registration: | N910BW |
MSN: | 40929 |
Total airframe hrs: | 195 hours |
Engine model: | Lycoming IO-540-T4B5D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Palatka Municipal Airport/Larkin Field (28J), Palatka, FL -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Palatka-Kay Larkin Airport, FL (28J) |
Destination airport: | Gatlinburg Airport, TN (GKT/KGKT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On July 18, 2022, at 0804 eastern daylight time, an experimental amateur-built RV-10 airplane, N910BW, was substantially damaged when it was involved in an accident near Palatka, Florida. The pilot was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
Shortly after takeoff, the experimental amateur-built airplane's engine lost total power and the pilot made an off-airport forced landing, resulting in substantial damage to the fuselage, both wings, and the tail section. Postaccident examination of the engine revealed that a cannon plug-type circular connector that connected the engine's electronic ignition system's wire harness to the two electronic control units was not properly connected. The manufacturer of the ignition system stated that disengagement of the connector, which carried all electrical signals required to run the ignition system, “…would result in a single point failure of the entire ignition system.' Maintenance records showed that the ignition system had been installed about 21 months before the accident, with no other work to that system detailed between that time and the accident. Based on this information, it is likely that the connector had not been fully secured when the system was installed, and that over time, the partial connection had loosened, ultimately resulting in the loss of engine power.
Probable Cause: Total loss of engine power due to the improper installation of an electronic ignition system connector plug.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA22LA322 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB ERA22LA322
https://data.ntsb.gov/Docket?ProjectID=105519 FAA register:
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=910BW https://flightaware.com/live/flight/N910BW/history/20220718/1125Z/28J/KGKT Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
18-Jul-2022 17:27 |
Geno |
Added |
18-Jul-2022 17:50 |
RobertMB |
Updated [Registration, Cn, Nature, Destination airport, Source, Narrative] |
18-Jul-2022 17:56 |
RobertMB |
Updated [Operator] |
16-Nov-2023 15:27 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report] |
16-Nov-2023 21:23 |
Captain Adam |
Updated [Time, Operator, Departure airport, Source, Narrative, Photo] |
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