ASN Wikibase Occurrence # 282616
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Date: | Wednesday 11 September 2019 |
Time: | 12:36 LT |
Type: | Piper PA-34-200T Seneca II |
Owner/operator: | Aircraft Resource Management, LLC |
Registration: | N328RG |
MSN: | 34-7570061 |
Year of manufacture: | 1975 |
Total airframe hrs: | 2752 hours |
Engine model: | Continental TSIO-360-EB1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Kingman, KS (9K8) -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Wichita Dwight D. Eisenhower National Airport, KS (ICT/KICT) |
Destination airport: | Kingman, KS (9K8) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was on a personal flight when, during final approach for landing, the gear unsafe warning horn sounded. The pilot made a go-around when he saw the gear safe indicator lights were not illuminated. The pilot verified, with another pilot on the ground, that the landing gear were not extended after several attempts to extend the landing gear, including using the emergency extension procedure. The pilot then made a wheels-up landing on the runway, during which the airplane's lower fuselage structural longerons were substantially damaged.
After the accident, the landing gear extended into the down-and-locked position when the airplane was hoisted off the runway surface using a crane and straps. Postaccident examination and testing revealed no issues with the normal landing gear extension/retraction system or the emergency extension procedure. The investigation was unable to duplicate the pilot's report that he was unable to extend the landing gear using the normal and/or emergency procedures during the flight. The reason for the malfunction of the landing gear extension system could not be determined based on the available evidence.
Probable Cause: The malfunction of the landing gear extension system for reasons that could not be determined with the available evidence.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA315 |
Status: | Investigation completed |
Duration: | 2 years and 11 months |
Download report: | Final report |
|
Sources:
NTSB CEN19LA315
Location
Revision history:
Date/time | Contributor | Updates |
09-Sep-2022 12:44 |
ASN Update Bot |
Added |
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