Accident Van's RV-7A N131RV,
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ASN Wikibase Occurrence # 284022
 
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Date:Friday 21 December 2007
Time:16:30 LT
Type:Silhouette image of generic RV7 model; specific model in this crash may look slightly different    
Van's RV-7A
Owner/operator:
Registration: N131RV
MSN: 70327
Total airframe hrs:290 hours
Engine model:Lycoming IO-360
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Elmendorf, TX (28TE) -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Houston-Weiser Air Park, TX (KEYQ)
Destination airport:Elmendorf, TX (28TE)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The private pilot landed his single-engine tricycle gear homebuilt airplane at a private 2,600-foot long by 200-foot wide grass airstrip. The pilot reported that on approach the airplane had about a 25-degrees of flap setting; he then "slowed [the airplane] to 80 knots on final [and crossed] over the fence at 70-75 knots." The pilot added, he made a normal landing and held the aircraft's nosewheel off the surface of the runway, until the airspeed bled off. About halfway down the runway, he stated that the airplane's nose suddenly lifted to about a 25-30 degree angle and when the nose came back down, he felt a "shutter". After the nosewheel came in contact with the runway surface, the aircraft tipped forward and while at a very slow speed, flipped over. The aircraft came to rest in the inverted position. The pilot inspected the runway and reported that about 66-feet from the aircraft, it appeared the nosewheel contacted the side of a "gopher mound" which caused the aircraft's nose to elevate. About 36-feet from the mound, and about 6-feet from where the nosewheel contacted the surface, the nosewheel track showed signs of widening. The wheel track got progressively wider and deeper until the point where the aircraft overturns. The aircraft had not been modified with the kit manufacturer's service bulletin, which increased the nose fork axle-to-ground clearance; the pilot added that he didn't think the added clearance would have helped prevent the accident.

Probable Cause: The failure of the nose landing gear. A contributing factor was the mound/uneven runway surface.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DFW08CA048
Status: Investigation completed
Duration: 2 months
Download report: Final report

Sources:

NTSB DFW08CA048

Revision history:

Date/timeContributorUpdates
30-Sep-2022 06:45 ASN Update Bot Added

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