ASN Wikibase Occurrence # 284783
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Date: | Sunday 10 June 2007 |
Time: | 18:30 LT |
Type: | Cessna 172RG |
Owner/operator: | Corkins Research LLC |
Registration: | N522GC |
MSN: | 172RG0091 |
Year of manufacture: | 1979 |
Total airframe hrs: | 3088 hours |
Engine model: | Lycoming O-360-F1HG |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lantana, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Daytona Beach International Airport, FL (DAB/KDAB) |
Destination airport: | Palm Beach-Palm Beach County Airport, FL (LNA/KLNA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that the landing gear would not go down, and there was no green indication for the landing gear indicators. He said he looked out the left window and the main gear was not extended, and that attempts at lowering the landing gear caused the circuit breaker to "trip." Pushing the circuit breaker back in was also ineffective in lowering the landing gear. He said he initiated emergency procedures to extend the landing gear, and the hand pump also failed to extend the landing gear. After recycling and pumping the landing gear for about 20 minutes, he said that it became clear to him that the landing gear would not extend, and he did not know if the right main and nose gear were extended. During the landing he said that he slowly brought the airplane to the ground so as not to cause a propeller strike, and later found that the landing gear was partially extended, causing the airplane to veer off the runway into the rough gravel and sand, incurring damage. After recovery the airplane was examined by an FAA licensed airframe and powerplant mechanic, who found that the hydraulic line on the down-lock side of the nose actuator had separated at the fitting, which had resulted in a total loss of hydraulic fluid, and the landing gear collapsing.
Probable Cause: Separation of a landing gear hydraulic line at the fitting for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA07LA109 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB MIA07LA109
Revision history:
Date/time | Contributor | Updates |
01-Oct-2022 07:29 |
ASN Update Bot |
Added |
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