ASN Wikibase Occurrence # 284809
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Date: | Wednesday 6 June 2007 |
Time: | 10:00 LT |
Type: | Air Tractor AT-401 |
Owner/operator: | Whittington Air |
Registration: | N92PK |
MSN: | 401-0821 |
Year of manufacture: | 1991 |
Total airframe hrs: | 4680 hours |
Engine model: | Pratt & Whitney R-1340 ANI |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Oak Grove, Louisiana -
United States of America
|
Phase: | Unknown |
Nature: | Agricultural |
Departure airport: | Eudora, AR |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The 5,475-hour commercial pilot reported that after performing an aerial application pass in his radial-engine-powered airplane, he initiated a turn to reverse direction to start another pass. At the top of the turn, he heard a loud bang from the radial engine, followed by the sound of the engine winding down. He also noticed white smoke from the exhaust, a loss of power, and a drop in manifold pressure. The pilot made an forced landing to a field, where the airplane rolled about 250 yards before it flipped over. The airplane was released to the owner after the accident, who later sold it to another operator. Due to the damage sustained in the accident, the engine was disassembled and examined before the new owner could return the airplane back to service. The new owner provided an engine disassembly report. According to the report, "undetermined causes resulted in distress to the phenolic separator bracket of the rear impeller support bearing resulted in its separation and fragmentation." The reports adds that "this initiated a chain reaction of events throughout the rest of the engine as clearances, lack of lubrication and subsequent wearing of engine components took place." This damage ultimately resulted in destruction of the blower labyrinth seal and the impeller gear train, which reduced power output. The engine reports concludes that "the destroyed impeller drive gear train and the distress caused by the displaced blower spring drive mechanism, coupled with reduced power output, resulted in seizure of the propeller shaft/crankshaft and complete loss of power."
Probable Cause: A complete loss of power due to failure of the impeller drive gear train and displacement of the blower spring drive mechanism, which resulted in seizure of the propeller shaft/crankshaft. Also causal was the failure of the phenolic separator bracket of the rear impeller support bearing for undetermined reasons. A factor was the none suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW07LA138 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB DFW07LA138
Revision history:
Date/time | Contributor | Updates |
01-Oct-2022 09:05 |
ASN Update Bot |
Added |
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