ASN Wikibase Occurrence # 284824
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Date: | Saturday 2 June 2007 |
Time: | 12:15 LT |
Type: | Lancair IV-P |
Owner/operator: | |
Registration: | N401PT |
MSN: | LIV-408 |
Year of manufacture: | 2002 |
Total airframe hrs: | 860 hours |
Engine model: | Walter 601E |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Parowan, Utah -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Phoenix-Deer Valley Airport, AZ (DVT/KDVT) |
Destination airport: | Hailey-Sun Valley Airport, ID (SUN/KSUN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was about 1 hour 15 minutes into the flight, and the airplane was cruising at 26,000 feet, when the turbo prop engine lost power with white smoke coming out of the exhaust. About a minute before the pilot had observed what he termed "splats" of moisture on the windscreen. He performed an emergency descent and at 12,500 feet attempted an engine restart. The restart attempt was unsuccessful. He glided to the nearest airport, circled, and performed a power-off landing. The airplane crossed the runway threshold at 120 knots, floated, and touched down at mid field. After touchdown, the airplane continued down the runway, off the end, and into terrain and a fence. The airplane came to rest with the landing gear collapsed. Federal Aviation Administration inspectors examined the airplane, and could not identify any mechanical abnormality with the engine or fuel system. The Pilot Operating Handbook states that an engine relight was possible below 13,000 feet mean sea level, and below 160 knots of airspeed. The pilot could not recall what his airspeed was when he attempted the engine restart. The airplane was not equipped with any type of engine inlet anti-ice or deicing equipment. The pilot did state that he had been in and out of moisture while at his 26,000 feet cruising altitude, but there had been no ice buildup on his wings or windscreen. A technical representative for Lancair stated that a 3/4 blockage of the engine cowling NACA induction scoop might be enough to starve the engine of air and induce a flameout.
Probable Cause: A loss of engine power due to engine inlet icing. Contributing to the accident was the lack of engine inlet anti-icing capability.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX07LA184 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX07LA184
Revision history:
Date/time | Contributor | Updates |
01-Oct-2022 09:17 |
ASN Update Bot |
Added |
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