ASN Wikibase Occurrence # 284955
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 4 May 2007 |
Time: | 15:15 LT |
Type: | Piper PA-38-112 Tomahawk |
Owner/operator: | Private |
Registration: | N2600N |
MSN: | 38-79A0936 |
Year of manufacture: | 1979 |
Total airframe hrs: | 3899 hours |
Engine model: | Lycoming O-235 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Odenton, Maryland -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Allentown, PA (1N9) |
Destination airport: | Fort Meade/Odenton-Tipton AAF, MD (FME/KFME) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that the cross-country flight was uneventful until in the vicinity of his planned destination, and that there were no problems with the performance or handling characteristics of the airplane. As the airplane turned from a southerly heading to an easterly heading to align with the destination runway, the pilot switched fuel tanks, and the engine immediately stopped producing power. According to the pilot, "I made a mistake. I should have switched tanks while the wings were level, before I made the maneuver." The pilot again switched tanks, turned on the fuel boost pump, and attempted a restart, but lacked the altitude to accomplish the engine start. He then maneuvered the airplane to a two-lane road that ran parallel to a busy state highway beneath him for the forced landing. Examination of the airplane at the scene revealed that both fuel tanks were voided, but the fuel caps remained secure in their ports. There was no odor of fuel, nor was there evidence of fuel spillage at the scene. The left fuel gauge indicated one-half tank, and the right fuel gauge indicated "Empty." The fuel selector was selected to the right fuel tank position. According to the pilot, "I had plenty of fuel, I just didn't manage it right."
Probable Cause: The pilot's mismanagement of the airplane's fuel supply, which resulted in fuel starvation and a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC07FA109 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB NYC07FA109
History of this aircraft
Other occurrences involving this aircraft
30 June 1997 |
N2600N |
Raleigh Flying Service |
0 |
Smithfield, NC |
|
sub |
Revision history:
Date/time | Contributor | Updates |
01-Oct-2022 15:45 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation